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2007 Ford F150 XLT SuperCrew
(11th Gen 04-08)

Maintenance & Repair Log  |  Features & Specs  |  Home

Maintenance, Repair, & Improvements Log

 

Date Description of Work Done Odometer Engine Hours Parts Cost Labor Cost Total
Cost
Warranty Notes

Informational: Common problems on the 11th Gen F150s
https://www.youtube.com/watch?v=XilMYsWOTpo
 

Informational: Spark Plug Tips
FordTechMak https://youtu.be/PHQxnG6Bd3o

https://www.f150forum.com/f4/2007-5-4l-spark-plug-tips-516651/index2/
Misc notes:
Torque to 22 to 28 Ft. lbs (Rock Auto)
Next design SP515 1 piece design.
The latest ones are latest SP546
or autolite ht15
blow out the plug wells with air before removing the plugs so you don't get dirt in the cylinders, and to torque to 25 ft-lb
I have a 2005 f150 4x4 lariat and i suggest you do 2 things. Remove the coils and spray pb blaster down the holes and let them soak overnight then the next day get a spark plug socet and just bareley crack them like 1/8 th of a turn and then go get the spark plug removal tool. At least 3 or 4 will break off. Ford says they are good for 100k miles, i change mine every 50k. Use antiseize thread compound when changing.
Others say use carb cleaner & use a stubby impact wrench on warm engine to remove.
I used Ford's (Motorcraft) nickel-based anti-seize and a torque wrench
Lisle 65600 broken spark plug removal tool
 
FUTURE
Top End Engine Work
Replace all roller followers (esp passenger side where oil is starved)
Maybe also the lash adjusters
Timing chain tensioners
Cam Phasers
Melling higher volume oil pump
Intake manifold (maybe)
Ford Tech M https://www.youtube.com/watch?v=xkkCzUVme_Y
 
FUTURE
Front Axel Fluid Change
How-to: https://www.youtube.com/watch?v=f0MhOijZS7o
Fluid to use: Motorcraft SAE 80W-90 Premium Rear Axle Lubricant
Capacity: 3.7pints = nearly 2 qts
Torque fill port to 18ft lbs
 
FUTURE
Differential Fluid Change  CHECK EXISTING FLUID FIRST TO SEE HOW DIRTY IT IS
How-to: https://www.youtube.com/watch?v=-LIm-YZ4DUI
Use Permatex 81182 Gear Oil RTV Gasket Maker
Tighten differential cover to: 35ft lbs. No torque sequence.
Diff fluid to use as "everything changed over: Synthetic 75W-140
Capacity: 3-3.5qts
Differential: 3.55 Limited Slip (per H9 code on door sticker): Add friction modifier XL-3
Torque fill port to 18ft lbs
(All materials purchased 12/6/23)
 
FUTURE
Transfer case drain & refill
How-to: https://www.youtube.com/watch?v=Sd-0tit_ZAI
Torque spec is critical to avoid splitting the case: 17ft lbsf
Use Motorcraft Mercon LV (do NOT use Mercon V, and Mercon is no longer being made)
Capacity approx 2qts.
Recommends draining & filling every 30,000k
 
FUTURE
Put a wire mesh screen over air intake to keep rats from entering side air intake assembly.

Drain / flush transmission, change filter, clean magnet, and install pan with plug.
FUTURE
Transmission Service
Motorcraft XT5QMC Mercon 5 Automatic Transmission Fluid
Motorcraft FT-105 Filter Assy (no gasket)
Dorman 265-813 Transmission Pan with drain plug
 
4/15/24
Added about 1 gallon of 50/50 gold coolant to reservoir to bring it up to the mark.
 


 
4/9/24
Screeching noise from front of vehicle (different from belt tensioner).

JPOST: https://www.f150forum.com/f4/screeching-under-hood-area-557291/#post7585069

JPOST: https://www.f150forum.com/f4/urgent-4r75e-possible-transmission-trouble-557090/#post7583020

JPOST: https://www.crownvic.net/ubbthreads/ubbthreads.php?ubb=showflat&Number=4183357&#Post4183357
 

122,500?
4/9/24
Belt Tensioner Failure
I found the bearing for the pulley of the belt tensioner completely missing; the tensioner had butted up against the passenger timing chain cover and wore a shallow groove into it.

Replaced BT with Motorcraft BT165(?) & serpentine belt with Gates K061031 / 6PK2618.
 

122,500 squeel noticed

122,962 repair completed
4/7/24
Misfires consistently reported cylinder 1 under heavy load > 3000RPM (mountain driving).
Replaced COP for cylinder 1 (Motorcraft) and the problem did not return although cylinder 3 has begun doing the same.  DG511 / 3L3Z-12029-BA / 3L3E-12A366-CA

Checked trans fluid for the first time ever: It was at the bottom of the crosshatch. Added 1 qt SuperTech Mercon V, and a second qt just to get more fresh fluid in there.
 

122,560
12/31/23
The battery seems like it may be getting weak, already.
 
12/10/23
Random / unprovoked addition of a bit of R134A refrigerant to the AC system.
 
11/12/23


At cold startup, truck has not been rattling like it use to.

Added Gunk Motor Flush cleaner to oil and ran truck for 31 minutes, mostly at idle, but I did rev it a few times.   The recommended time to run vehicle is 5 minutes but I ran it longer to help fully loosen anything up.

Changed oil and filter; oil = 6qt Rural King 5W20 Full Synthetic + 1 heaping quart of Lucas;  filter=Motorcraft FL-820S.  This is the first time I have ever used Lucas.    The old oil didn't appear to have any grit or foreign particles in it other than being quite dark, which part of that may be the varnish that the Gunk Motor Flush loosened up and dissolved.  I installed oil pan drain plug using a new cut piece of cork gasket.  Engine sounded no different while running after the oil change. 
 

119,768
7/20/23
Cold Startup Rattle
Since purchased, upon cold startup, the engine has always had a sever rattle for a few seconds.

Youtube: Ford 5.4L 3v Engine Noises You Shouldn’t Ignore: How To Tell When a Timing Job is Really Needed

Youtube: Ford F-150 5.4L 3v Triton Engines: This is Why You Always Replace the Roller Followers!
 

5.4L 3V 2004-2010 Ford OEM Cam Phaser, Timing Chain, Upgraded Oil Pump, and VCT Solenoid Replacement Kit SKU# 3R2Z-6A257-DA-RAT-KIT  $1262


Consider using quart of Lucas oil additive and/or Marvel Mystery Oil. (I ordered Lucas)

Consider 10W30 or 5W30 for next oil change. Someone suggested 0W40
FordTechMakuloco: "many are using 15w-40 no problems but I recommend 5w-30"
NO> JUST USE 5w20 (spec) and add make the oil 20% Lucas.  20% of 7qts is 1.4qts.

Tip for taking out spark plugs without breaking them: Kroil & work them easy with 3/8in impact wrench.  Actually, this TSB covers the proper way to remove spark plugs.

7/22/23> Ran truck & recorded startup where is makes that racket for a couple of seconds. Truck hasn't run in a week.

Truck engine sounds good; there is no thuds or any odd noises.  It ticks & purs seemingly like it should,  thankfully.  So I don't think there are any cam problems at this point like I've read seen online lately with these 5.4s - just likely leaky hydrolic timing chain tensioners. 

 I looked down into the oil fill neck, and there seems like there could be varnish on some of the metal inside.  It seems plausible that a good oil flush additive might help remove some grime/sludge which is so crucial for these vehicles with variable timing and small oil holes on the cam components. .

7/29/23 SAT> When I started up the truck today after it sat for a week again, interestingly, it did NOT make any startup rattle at all.

9/1/23 Truth be told, I don't see why I can't run straight 10w30 oil in this engine due to hot temps nearly year-round here in FL.

11/5/23 Ran truck today after it sat over a week. It had NO startup rattle at all. 
After warmed up and at idle, it has some ticks, but it doesn't seem all that significant.  I am not terribly worried about this engine at this time. But as everyone says, do change the oil on time because any junk in the oil will block the upper end passages and cause further wear.


 

7/2/23
Replaced Horns
I replaced both left set and right set of horns.  HOWEVER, I found that the old horns were not defective at all.  Instead, I do believe it is a power delivery issue; I believe the horns are not getting enough power from the skinny chassis wiring.  An easy partial-fix I implemented was I grounded the negative side of the horns to the frame.  These new horns sound a little better, but still seem to struggle to get enough power to sound right.
 
6/24/23
Horns Bad
After spending over an hour trying to find good quality horns, I decided to just order an exact replacement set of SyoAuto & Farbins.  Hopefully these last longer than a month.
(SEE ABOVE - THE HORNS ARE NOT THE PROBLEM)
 
6/23/23
Code P0420 logged.
"A P0420 code is set when the upstream sensor and the downstream oxygen sensor sense the catalytic converter is not doing its job. Basically, the amount of oxygen going into the converter is not being burned, and it detects it through the downstream sensor."
I cleared the code.

Update 6/24/23> P0420 came back.
10/26/23> I cleared the code again.
 

5/28/23
Replaced Starter
Price to replace starter, quoted from Firestoneyesterday: $374
Instead, today I went to Advance Auto on CC PKWY, and got a replacement starter under warranty (limited lifetime warranty) (Carquest 6646SN).   Since I purchased the last starter online, the clerk couldn't find my purchase in his system, and I pulled it up on my email.  He wanted to know the purchase price ($192.99) since online you typically get a discount.  He set up the swap differently from a refund/repurchase; he somehow did it as a no-receipt return and used my drivers license. He did this so I would not have to pay anything because he said it is that way when you buy it online.

I put my mind to replacing the starter, remembering how much of a pain it was last time. I watched a few youtube videos, and got it done.  The top bolt was difficult but not as bad as I remember last time.  Use 3/8in drive, deep & shallow 13mm sockets, and a combination of short and long extension with the swivel head 3/8in drive, and it can be done (For that top bolt
I think I used a long socket, 3in extension, another 3in extension, and a swivel head 3/8in drive, but I don't recall specifically).  Jack up truck at least 5in, jack stands under front wheel suspension arms, get under truck with feet toward driver's side.

The truck cranks perfectly now.
 

119,289
5/7/23
Battery Problem
This RK battery installed 1/5/23 is cranking truck weakly, and confirmed that it is weak and below 12v after vehicle is run.

Replaced it with Everstart Maxx 65N (Walmart).  SN: JCH20092916973
(The "N" means north for more cranking amps, and the "S" means south.)
Taking a chance with Walmart batteries again, so we'll see how well this one does.
Warranty: 3yr Replacement (confirmed with clerk in Automotive dep't: no pro rated warranty)
I did NOT take a picture of the side label of the battery before installation.

Starter was not as flaky today as it has been in the past.
 

119,288
1/5/23
Battery Problem
Had to jump battery today only a few days after it ran last.
Found that battery is weak and when engine is shut off it drops to just below 12volts.
Returned the 6 month old battery to RK and purchased a new one.
The new one is only 60mth / 1 yr free rplcmnt since the "better" one wasn't in stock.

Update 1/6/23> Installed new battery, and truck cranks very well now.
Also, topped off oil, and coolant (used G05 Zerex as that is what most google answers said).
 

10/30/22
Starter Sticking
11/22/22 Update> The starter is not sticking anymore and has been consistently cranking on  the first try.

11/23/22> It stuck a couple times today.
 

10/20/22
Steering Binding
Steering binded up and was uneven while turning the steering wheel.
A youtube video revealed that the two steering shaft U-Joints are to blame.
I spray-oiled them and the steering went back to normal again - smooth like before.
 
10/16/22
H. Ian hit us 9/28/22
We drove through deep salt water on 9/28/22.  A week or two later the starter wouldn't engage.  I tapped the starter and shorted the terminals - it sparked alot and then eventually the starter began spinning and is working now.

I replaced the blown 20amp horn fuse with a 25amp fuse.  I also disconnected the two red horns.  The existing new horns sound terrible already.  I don't know how they could have gone bad so fast except if somehow rain from H. Ian got into them already, or they are just poor quality horns. 
(I ended up setting up a return/refund for both sets of horns, but apparently I never returned them, likely due to the chaos that I was involved in at the time with regard to Hurricane Ian that happened weeks earlier.) Stay away from these branded horns: SyoAuto, Farbin, Wolo.
Update 6/26/23: After spending over an hour trying to find good quality horns, I decided to just get an exact replacement set of SyoAuto & Farbins.

10/19/22> Blew out starter and solenoid with compressed air.  Also forced spray-lube up drain holes in solenoid and starter. 

10/20/22> Starter continues to be sluggish and sometimes wont start without a second key turn.

10/30/22> The truck starter has been seizing up again if it sits a week.
Today, I stuck a skinny red tube through the port that the starter's positive cable goes through and pumped it full of spray oil until it started coming out the starter and solenoid drain holes. I then shorted the terminals and spun the starter quite a bit.  Hopefully this helps for the long-term.
 

9/24/22
Replaced the 2 red crappy horns put on about 10 months ago with a set of two horns, and and additional set of 2 horns, both of different brands, from Amazon.

Update 9/24/22: Added the 2 red horns back on, so now there is a total of 6 horns which may overload the 20A circuit.  The plan would be to put a 30A fuse in if the 20A fuse blows.  The circuit is a brief-usage, so I think this up-rating of the circuit is OK.

Added some G05 coolant to the coolant recovery tank as it was quite low.
 

9/5/22
Noticed and pulled a broken-off nail from LR tire toward outside of tread.  There was no hissing so I did not plug or patch it. To observe if there is any pressure loss over the next few days.
 
7/30/22
AC Service
In the heart of the summer, I topped off refrigerant in AC system.  It was nothing scientific, but added 4 or 5 x 10 second blasts of refrigerant which seemed to help inside low temperature blow a little.
 
118,186
7/24/22
Installed replacement bolt/nut onto lower left area of cap glass.
A second bolt/nut set is in the glove box for when it comes time to replace the right assemply.
 
6/21/22
Battery Replacement
6/20/22 > Purchased 07F150 Battery Group 65 2yr/72m @89.99 SN:25640987
6/21/22> Installed this new battery.
 
118,155
6/18/22
Battery Weak
After a couple of weeks, the truck needed a jump to start.
It also cranks weak now.
Load testing it shows that the battery appears weak.
The battery is only 2y4mth old.
It is likely time to replace the battery. RK has one with 3y/72mth warranty for $90.
 
6/4/22  
Installed a brand new locking fuel cap. Stant 10510.
Code on cap & keys: 12EL
 

6/1/22
 

Fuel Economy Summary
I figured out that just putzing around town, local/nearby short trips, the truck is getting only 5.5mpg.  Terrible!
Nearby short trips: 5.5mpg  (at current fuel rates that's $0.83/mile)
City: 10mpg
Hwy: 17mpg
 
5/14/22
Rear cap glass is coming lose due to a rusted washer. It is a Jason cap, but the only results that come up for the part is a search for  Leer Button Stud Kit 51454.
Available here but $40 min purch to avoid outrageous $25 shipping fee:
https://www.izzwanw.com/truck-cap-leer-windowdoor-2-large-buttons-51454-complete-with-washers-and-nut-p-569651.htm
 
4/16/22
Installed 6 gauge / 60 amp circuit from battery to center console to power inverter.
It also reaches underneath right side near frame rail so that if I ever want to install a battery there onto the frame rail I can.

Blew a 20amp cigarette lighter cartridge fuse tonight.
Spent alot of time trying to determine the fuse types on this truck.
It appears to have both mini fuses and tall (27mm) cartridge fuses - no short cartridge fuses.
The passenger side fuse panel has these cartridge fuses: 4 X 20A, 8 X 30A, and 1 X 40A.
I ordered an assortment of tall cartridge fuses from Amazon.
 

4/8/22
The truck cap glass suddenly droops and won't stay up.
Numbers on both gas struts: Lift-O-Mat 003515 0200N 106/14 A 27
00691018

I measured approx 15.6in extended X approx 10.5 compressed.
Found some similar replacements on Amazon for $20 a pair and ordered. them.
 


1/9/22
 

Truck Won't Start
Starter failed while Karla, Carlos, and I were at a club in Fort Myers.  Had to get towed by AAA.

1/10/21> Removed starter.   The top bolt is very difficult to get to but it can be done with the right socket extension lengths.
Replaced starter with Carquest 6646SN limited lifetime warranty (Advance Auto) which had better ratings than the units at Autozone, and I didn't want to wait for Amazon.
 

117,8??
1/3/22
Replaced torn air filter (previously chewed by rats) with Super Tech (#1340).

Filled fuel tank post trip 16.06gal. 117,542:  17.1mpg
 

117,542
1/1/21 - 1/2/21
621-mile trip around Florida
Began: 116,910 (filled fuel tank shortly after)
Coleman FL: Filled fuel tank 11.6gal. 117,110: 17.2mpg
South of Cocoa Beach FL: Filled fuel tank 10.95gal. 117,267:  14.3mpg
 
12/30/21
Problem with truck stalling out.
Truck was idling in a parking lot with AC on and suddenly started to run bad and stall out even after startup. I was able to drive it home luckily.

Numerous codes were being logged:
P2195 -02 Sensor Signal Stuck Lean Bank 1
P0174 - Too Lean Bank 2
P0301 - Cylinder 1 Missing

Hooked up the Elm Scan & computer with ODB Wiz to read the different parameters of the ECM.

Then later, only P0191 kept logging:
P0191 - Fuel Rail Pressure Sensor Circuit Range/Performance
(Fuel rail pressure sensor on vehicle: 5C3E-9G756-AC)

Research suggested that either the FRPS is bad or the Fuel Pump Driver Module (on vehicle: 5L8A-9D370-AA) is bad or the fuel pump is bad, or some or all of these.  I noticed when I unplugged FRPS the engine ran better.  Therefore,  I had a hunch the FRPS was bad.  I purchased a replacement, installed it, and now the engine seems to run right. Duralast SU8744.
I also read that the FRPS has a fuel temperature sensor in it.

AC Service
I noticed the AC compressor cuts out alot.
AC on max, the low side pressure was 30psi.  I added R134a and brought the pressure to an arbitrary number: 45psi.

MPG Measurement
With the Elmscan hooked up and connected to laptop, I was able to record some MPG readings at different steady speeds with AC off:
30mph: 23.5mpg
40mph: 22mpg, 23.3mpg
45mph: 24mpg
So in general, from 30mph to 45mph, the truck gets about 23mpg .

 

116,850(?)
12/30/21
Removwd the ladder rack from the roof rack as it is not useful to us and could be in the way in the future.
Broke the right rear bolt holding the rear left-to-right rack.  It has been loose but I twisted the head off trying to tighten it.   Used a slightly bigger (1/4in) stainless steel bolt from the hardware store and forced it in (phillips head).
 
12/28/21
Removed the rear differential fill plug.  The magnetic plug was gummed up with thick sludge and filings.  Used my pinky and noticed the diff level was a bit low, but the fluid looked rather clean (brown and clear). 
Added about 1/2 qt of 85W140 gear lube.  Afterwards, a test drive proved no difference in differential whine.
 
116,839
12/27/21
Tax Collectors Office:
-Title transfer to my name.
-Registration

12/23/21> Got insurance on it.

The F150 is now legal to be driven on the road.
 

12/23/21
Left truck cap windows latch cable came loose.  Drilled it out. Used a cable clamp on the cable and crushed it in place.  Added a cable clamp to right side latch also.

Ran wire from under driver side frame to cap's 3rd / middle brake light (LED) which had never been hooked up.
3rd brake light in cap is model AT-LED-28X30-01 & CT-14008319.

Noted the model of the bed cap is: Jason Industries Inc. 367804 "Cyber Skirt 2, Tricell, Carpet"
"04-08 FORD".

Noticed the engine isn't running right. It is also bogging down some when I floor it while driving.
I think water got into the ignition plug boots, from me washing out the engine yesterday. Took all ignition plug boots off and blew out the spark plug wells and boots. Many were wet. Also removed fuel injector connectors and blew out both sides.
Engine runs noticeably smoother and acceleration responsiveness is back to normal.
Note: DONT WASH DOWN ENGINE anymore like I did yesterday. Blow it out with compressed air instead.

Noted the length of the bed with the tailgate shut is right at about 67in (5ft 7in).

Checked the oil: It is full and looks clean.
 

116,787
12/22/21
Fully cleaned up the entire truck outside and inside, including the bed which was filthy with wetness, rocks, mud, bolts, and nails under the flat bed mat that was on top the bed liner. Also washed down engine compartment as there was lots of rat feces & grass & twigs brought in by rats.  Saw a rat under the hood as I opened it.

Also, should probably park the truck at a rear-downward slope as I think the cap may leak just a little, and water accumulates at the front of the bed if not sloped back to allow it to drain.

Horn did not work so replaced with Wolo Maxi Sound 2 Horn Set #320-2T. They are OK; they are not quite as loud as I'd like. Apparently they are "150db".
(9/23/22 These horns suck)

Replaced windshield wipers. Brand Carquest  XQ20.
 

9/11/21
RR tire looses air faster than the rest.
 
3/8/20
Changed oil and filter; oil = 7qt Rural King 5W20 Full Synthetic;  filter=Motorcraft FL-820S.

Engine made quite a clanking sound at startup for about 2 seconds until oil was circulated.
 

116,742
2/23/20
Mileage logged.

JCA will be using it for work this week.

Oil needs to be changed.

3/2/20> Calculated that the 4 days I used the truck for work commute I got average of 12.5mpg.
 

116,558
approx 2/17/20
AKA had battery replaced.
Duralast 52948596046 which appears to have a 2 year warranty.
 
1/16/20
to
2/4/20

Trip to Rhode Island & back
 
12/15/19
SUN

Coolant recovery tank coolant level has not dropped at all. 
 
12/9/19
MON

Coolant recovery tank seems to be holding coolant now. To keep observing.
 
12/8/19
Current tires on vehicle are Mastercraft Courser HXT
Size: LT275 65 R18
Tires are worn evenly.
There is a spare under the bed.

Topped off coolant recovery tank again.

Inspected underside extensively:
-FR CV joint boot is torn and needs to be replaced.

Topped off air in tires to 35lbs.

Checked oil again: It is a bit overfilled.
 

110,975
12/7/19
Cooling system has a lot of orange sludge in it and the coolant is orange/rust colored.
Cleaned out coolant recovery tank and topped off coolant.
Searched internet forums. About half say the sludge is normal, and the other half say it is not.

Oil seemed to be a bit low so added approx 1/2 qt RK 10W30 conventional oil.

Tested 4WD (4H & 4L): It works good.

I believe the high-speed road noise is coming from the differential  (or transfer case?). Should pull diff cover at some point and at the very least change the fluid.
 

12/8/19
Vehicle seems like it may be losing some coolant.
 
12/5/19
THU

AKA found vehicle on Facebook advertised for sale.
We went to Port Charlotte to inspect it.

Fuel filter underneath is shiny (and therefore likely new-ish).

Coolant overflow tank has orange sludge in it. No sign of water in the oil.
Coolant is low - overflow tank only has about an inch of coolant in it.

Noticed lots of noise seeming coming from tires at 50mph + (No not the tires).

Purchased vehicle from Terry.
 

Approx.
110,895

 

Maintenance Items Cross Reference/ Specs
 


Fuel tank 27gal (or 30 possibly but likely 27)
Coolant: "Motorcraft Premium Gold Engine Coolant with bittering agent (yellow-colored)"
"VC-7-B / WSS-M97B51-A1"
The Zerex G-05 is suitable coolant compatible with this vehicle.


Door Sticker Tire Size: P275 65 R18
Tire Inflation Pressure (cold): 35lbs front & rear
Oil weight: 5W20
Oil capacity: 7qts
Oil filter: FL-820S
Air Filter: FA-1754
Fuel Filter:
Transmission:4R75E
4R75E note: "-A sealed case and lifetime transmission fluid make the transmission maintenance free, while adaptive pressure control maintains consistent shift feel over time."Automatic Transmission Fluid: XT-5-QM / MERCON V
ATF capacity: 13.9qt
Transfer Case Fluid: XT-2-QDX / MERCON
Transfer Case capacity: 2qt
Transmission Pan Bolt Torque: 10ft lbs (per 2 separate youtube video)

Flex Fuel capable?: Unclear. "If your vehicle is FFV capable, it may have a yellow colored fuel cap."

 

 

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