AFW
2007 Ford F150 XLT SuperCrew |
Maintenance, Repair, & Improvements Log
Date | Description of Work Done | Odometer | Engine Hours | Parts Cost | Labor Cost | Total Cost |
Warranty | Notes |
Informational: Common problems on the 11th Gen F150s https://www.youtube.com/watch?v=XilMYsWOTpo |
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Informational: Spark Plug Tips FordTechMak https://youtu.be/PHQxnG6Bd3o https://www.f150forum.com/f4/2007-5-4l-spark-plug-tips-516651/index2/ Misc notes: Torque to 22 to 28 Ft. lbs (Rock Auto) Next design SP515 1 piece design. The latest ones are latest SP546 or autolite ht15 blow out the plug wells with air before removing the plugs so you don't get dirt in the cylinders, and to torque to 25 ft-lb I have a 2005 f150 4x4 lariat and i suggest you do 2 things. Remove the coils and spray pb blaster down the holes and let them soak overnight then the next day get a spark plug socet and just bareley crack them like 1/8 th of a turn and then go get the spark plug removal tool. At least 3 or 4 will break off. Ford says they are good for 100k miles, i change mine every 50k. Use antiseize thread compound when changing. Others say use carb cleaner & use a stubby impact wrench on warm engine to remove. I used Ford's (Motorcraft) nickel-based anti-seize and a torque wrench Lisle 65600 broken spark plug removal tool |
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FUTURE | Top End Engine Work Replace all roller followers (esp passenger side where oil is starved) Maybe also the lash adjusters Timing chain tensioners Cam Phasers Melling higher volume oil pump Intake manifold (maybe) Ford Tech M https://www.youtube.com/watch?v=xkkCzUVme_Y |
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FUTURE | Front Axel Fluid Change How-to: https://www.youtube.com/watch?v=f0MhOijZS7o Fluid to use: Motorcraft SAE 80W-90 Premium Rear Axle Lubricant Capacity: 3.7pints = nearly 2 qts Torque fill port to 18ft lbs |
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FUTURE | Differential Fluid Change CHECK EXISTING FLUID FIRST TO SEE HOW DIRTY IT IS How-to: https://www.youtube.com/watch?v=-LIm-YZ4DUI Use Permatex 81182 Gear Oil RTV Gasket Maker Tighten differential cover to: 35ft lbs. No torque sequence. Diff fluid to use as "everything changed over: Synthetic 75W-140 Capacity: 3-3.5qts Differential: 3.55 Limited Slip (per H9 code on door sticker): Add friction modifier XL-3 Torque fill port to 18ft lbs (All materials purchased 12/6/23) |
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FUTURE | Transfer case drain & refill How-to: https://www.youtube.com/watch?v=Sd-0tit_ZAI Torque spec is critical to avoid splitting the case: 17ft lbsf Use Motorcraft Mercon LV (do NOT use Mercon V, and Mercon is no longer being made) Capacity approx 2qts. Recommends draining & filling every 30,000k |
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FUTURE | Put a wire mesh screen over air intake to keep rats from entering side air intake assembly. Drain / flush transmission, change filter, clean magnet, and install pan with plug. |
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FUTURE | Transmission Service Motorcraft XT5QMC Mercon 5 Automatic Transmission Fluid Motorcraft FT-105 Filter Assy (no gasket) Dorman 265-813 Transmission Pan with drain plug |
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4/15/24 | Added about 1 gallon of 50/50 gold coolant to reservoir to bring it up to the mark. |
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4/9/24 | Screeching noise from front of vehicle (different from belt tensioner). JPOST: https://www.f150forum.com/f4/screeching-under-hood-area-557291/#post7585069 JPOST:
https://www.f150forum.com/f4/urgent-4r75e-possible-transmission-trouble-557090/#post7583020
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122,500? | ||||||
4/9/24 | Belt Tensioner Failure I found the bearing for the pulley of the belt tensioner completely missing; the tensioner had butted up against the passenger timing chain cover and wore a shallow groove into it. Replaced BT with Motorcraft BT165(?) &
serpentine belt with Gates K061031 / 6PK2618. |
122,500 squeel
noticed 122,962 repair completed |
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4/7/24 | Misfires consistently reported cylinder 1 under heavy load > 3000RPM (mountain driving). Replaced COP for cylinder 1 (Motorcraft) and the problem did not return although cylinder 3 has begun doing the same. DG511 / 3L3Z-12029-BA / 3L3E-12A366-CA Checked trans fluid for the first time ever: It was at the
bottom of the crosshatch. Added 1 qt SuperTech Mercon V, and a second qt
just to get more fresh fluid in there. |
122,560 | ||||||
12/31/23 | The battery seems like it may be getting weak, already. |
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12/10/23 | Random / unprovoked addition of a bit of R134A refrigerant to the AC system. |
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11/12/23 |
Added Gunk Motor Flush cleaner to oil and ran truck for 31 minutes, mostly at idle, but I did rev it a few times. The recommended time to run vehicle is 5 minutes but I ran it longer to help fully loosen anything up. Changed oil and filter; oil = 6qt Rural King 5W20 Full Synthetic + 1
heaping quart of Lucas; filter=Motorcraft FL-820S. This is the
first time I have ever used Lucas. The old oil didn't
appear to have any grit or foreign particles in it other than being quite
dark, which part of that may be the varnish that the Gunk Motor Flush
loosened up and dissolved. I installed oil pan
drain plug using a new cut piece of cork gasket. Engine sounded no
different while running after the oil change. |
119,768 | ||||||
7/20/23 | Cold Startup Rattle Since purchased, upon cold startup, the engine has always had a sever rattle for a few seconds. Youtube: Ford 5.4L 3v Engine Noises You Shouldn’t Ignore: How To Tell When a Timing Job is Really Needed Youtube:
Ford F-150 5.4L 3v Triton Engines: This is Why You Always Replace the Roller
Followers!
Consider 10W30 or 5W30 for next oil change. Someone suggested 0W40 Tip for taking out spark plugs without breaking them: Kroil & work them easy with 3/8in impact wrench. Actually, this TSB covers the proper way to remove spark plugs. 7/22/23> Ran truck & recorded startup where is makes that racket for a couple of seconds. Truck hasn't run in a week. Truck engine sounds good; there is no thuds or any odd noises. It ticks & purs seemingly like it should, thankfully. So I don't think there are any cam problems at this point like I've read seen online lately with these 5.4s - just likely leaky hydrolic timing chain tensioners. I looked down into the oil fill neck, and there seems like there could be varnish on some of the metal inside. It seems plausible that a good oil flush additive might help remove some grime/sludge which is so crucial for these vehicles with variable timing and small oil holes on the cam components. . 7/29/23 SAT> When I started up the truck today after it sat for a week again, interestingly, it did NOT make any startup rattle at all. 9/1/23 Truth be told, I don't see why I can't run straight 10w30 oil in
this engine due to hot temps nearly year-round here in FL.
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7/2/23 | Replaced Horns I replaced both left set and right set of horns. HOWEVER, I found that the old horns were not defective at all. Instead, I do believe it is a power delivery issue; I believe the horns are not getting enough power from the skinny chassis wiring. An easy partial-fix I implemented was I grounded the negative side of the horns to the frame. These new horns sound a little better, but still seem to struggle to get enough power to sound right. |
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6/24/23 | Horns Bad After spending over an hour trying to find good quality horns, I decided to just order an exact replacement set of SyoAuto & Farbins. Hopefully these last longer than a month. (SEE ABOVE - THE HORNS ARE NOT THE PROBLEM) |
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6/23/23 | Code P0420 logged. "A P0420 code is set when the upstream sensor and the downstream oxygen sensor sense the catalytic converter is not doing its job. Basically, the amount of oxygen going into the converter is not being burned, and it detects it through the downstream sensor." I cleared the code. Update 6/24/23> P0420 came back. |
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5/28/23 | Replaced Starter Price to replace starter, quoted from Firestoneyesterday: $374 Instead, today I went to Advance Auto on CC PKWY, and got a replacement starter under warranty (limited lifetime warranty) (Carquest 6646SN). Since I purchased the last starter online, the clerk couldn't find my purchase in his system, and I pulled it up on my email. He wanted to know the purchase price ($192.99) since online you typically get a discount. He set up the swap differently from a refund/repurchase; he somehow did it as a no-receipt return and used my drivers license. He did this so I would not have to pay anything because he said it is that way when you buy it online. I put my mind to replacing the starter, remembering how much of a
pain it was last time. I watched a few youtube videos, and got it done.
The top bolt was difficult but not as bad as I remember last time. Use
3/8in drive, deep & shallow 13mm sockets, and a combination of short and
long extension with the swivel head 3/8in drive, and it can be done (For
that top bolt The truck cranks perfectly now. |
119,289 | ||||||
5/7/23 | Battery Problem This RK battery installed 1/5/23 is cranking truck weakly, and confirmed that it is weak and below 12v after vehicle is run. Replaced it with
Everstart Maxx 65N (Walmart). SN: JCH20092916973 Starter was not as flaky today as it has been in the past. |
119,288 | ||||||
1/5/23 | Battery Problem Had to jump battery today only a few days after it ran last. Found that battery is weak and when engine is shut off it drops to just below 12volts. Returned the 6 month old battery to RK and purchased a new one. The new one is only 60mth / 1 yr free rplcmnt since the "better" one wasn't in stock. Update 1/6/23> Installed new battery, and truck cranks very well now. |
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10/30/22 | Starter Sticking 11/22/22 Update> The starter is not sticking anymore and has been consistently cranking on the first try. 11/23/22> It stuck a couple
times today. |
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10/20/22 | Steering Binding Steering binded up and was uneven while turning the steering wheel. A youtube video revealed that the two steering shaft U-Joints are to blame. I spray-oiled them and the steering went back to normal again - smooth like before. |
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10/16/22 | H. Ian hit us 9/28/22 We drove through deep salt water on 9/28/22. A week or two later the starter wouldn't engage. I tapped the starter and shorted the terminals - it sparked alot and then eventually the starter began spinning and is working now. I replaced the blown 20amp horn fuse with a 25amp fuse. I also
disconnected the two red horns. The existing new horns sound terrible
already. I don't know how they could have gone bad so fast except if
somehow rain from H. Ian got into them already, or they are just poor
quality horns. 10/19/22> Blew out starter and solenoid with compressed air. Also forced spray-lube up drain holes in solenoid and starter. 10/20/22> Starter continues to be sluggish and sometimes wont start without a second key turn. 10/30/22> The truck starter has been seizing up again if it sits a week. |
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9/24/22 | Replaced the 2 red crappy horns put on about 10 months ago with a set of two horns, and and additional set of 2 horns, both of different brands, from Amazon. Update 9/24/22: Added the 2 red horns back on, so now there is a total of 6 horns which may overload the 20A circuit. The plan would be to put a 30A fuse in if the 20A fuse blows. The circuit is a brief-usage, so I think this up-rating of the circuit is OK. Added some G05 coolant to the coolant recovery tank as it was quite low.
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9/5/22 | Noticed and pulled a broken-off nail from LR tire toward outside of tread. There was no hissing so I did not plug or patch it. To observe if there is any pressure loss over the next few days. |
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7/30/22 | AC Service In the heart of the summer, I topped off refrigerant in AC system. It was nothing scientific, but added 4 or 5 x 10 second blasts of refrigerant which seemed to help inside low temperature blow a little. |
118,186 | ||||||
7/24/22 | Installed replacement bolt/nut onto lower left area of cap glass. A second bolt/nut set is in the glove box for when it comes time to replace the right assemply. |
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6/21/22 | Battery Replacement 6/20/22 > Purchased 07F150 Battery Group 65 2yr/72m @89.99 SN:25640987 6/21/22> Installed this new battery. |
118,155 | ||||||
6/18/22 | Battery Weak After a couple of weeks, the truck needed a jump to start. It also cranks weak now. Load testing it shows that the battery appears weak. The battery is only 2y4mth old. It is likely time to replace the battery. RK has one with 3y/72mth warranty for $90. |
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6/4/22 | Installed a brand new locking fuel cap. Stant 10510. Code on cap & keys: 12EL |
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6/1/22 |
Fuel Economy Summary I figured out that just putzing around town, local/nearby short trips, the truck is getting only 5.5mpg. Terrible! Nearby short trips: 5.5mpg (at current fuel rates that's $0.83/mile) City: 10mpg Hwy: 17mpg |
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5/14/22 | Rear cap glass is coming lose due to a rusted washer. It is a Jason cap, but the only results that come up for the part is a search for Leer Button Stud Kit 51454. Available here but $40 min purch to avoid outrageous $25 shipping fee: https://www.izzwanw.com/truck-cap-leer-windowdoor-2-large-buttons-51454-complete-with-washers-and-nut-p-569651.htm |
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4/16/22 | Installed 6 gauge / 60 amp circuit from battery to center console to power inverter. It also reaches underneath right side near frame rail so that if I ever want to install a battery there onto the frame rail I can. Blew a 20amp cigarette lighter cartridge fuse tonight. |
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4/8/22 | The truck cap glass suddenly droops and won't stay up. Numbers on both gas struts: Lift-O-Mat 003515 0200N 106/14 A 27 00691018 I measured approx 15.6in extended X approx 10.5 compressed. |
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1/9/22 |
Truck Won't Start Starter failed while Karla, Carlos, and I were at a club in Fort Myers. Had to get towed by AAA. 1/10/21> Removed starter. The top
bolt is very difficult to get to but it can be done with the right socket
extension lengths. |
117,8?? | ||||||
1/3/22 | Replaced torn air filter (previously chewed by rats) with Super Tech (#1340). Filled fuel tank post trip 16.06gal. 117,542: 17.1mpg |
117,542 | ||||||
1/1/21 - 1/2/21 | 621-mile trip around Florida Began: 116,910 (filled fuel tank shortly after) Coleman FL: Filled fuel tank 11.6gal. 117,110: 17.2mpg South of Cocoa Beach FL: Filled fuel tank 10.95gal. 117,267: 14.3mpg |
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12/30/21 | Problem with truck stalling out. Truck was idling in a parking lot with AC on and suddenly started to run bad and stall out even after startup. I was able to drive it home luckily.
Numerous codes were being logged: Hooked up the Elm Scan & computer with ODB Wiz to read the different parameters of the ECM. Then later, only P0191 kept logging: Research suggested that either the FRPS is bad or the Fuel Pump Driver
Module (on vehicle: 5L8A-9D370-AA) is bad or the fuel pump is bad, or some
or all of these. I noticed when I unplugged FRPS the engine ran
better. Therefore, I had a hunch the FRPS was bad. I
purchased a replacement, installed it, and now the engine seems to run
right. Duralast SU8744. AC Service MPG Measurement |
116,850(?) | ||||||
12/30/21 | Removwd the ladder rack from the roof rack as it is not useful to us and could be in the way in the future. Broke the right rear bolt holding the rear left-to-right rack. It has been loose but I twisted the head off trying to tighten it. Used a slightly bigger (1/4in) stainless steel bolt from the hardware store and forced it in (phillips head). |
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12/28/21 | Removed the rear differential fill plug. The magnetic plug was gummed up with thick sludge and filings. Used my pinky and noticed the diff level was a bit low, but the fluid looked rather clean (brown and clear). Added about 1/2 qt of 85W140 gear lube. Afterwards, a test drive proved no difference in differential whine. |
116,839 | ||||||
12/27/21 | Tax Collectors Office: -Title transfer to my name. -Registration 12/23/21> Got insurance on it. The F150 is now legal to be driven on the road. |
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12/23/21 | Left truck cap windows latch cable came loose. Drilled it out. Used a cable clamp on the cable and crushed it in place. Added a cable clamp to right side latch also. Ran wire from under driver side frame to cap's 3rd / middle brake light
(LED) which had never been hooked up. Noted the model of the bed cap is: Jason Industries Inc. 367804 "Cyber
Skirt 2, Tricell, Carpet" Noticed the engine isn't running right. It is also bogging down some when
I floor it while driving. Noted the length of the bed with the tailgate shut is right at about 67in (5ft 7in). Checked the oil: It is full and looks clean. |
116,787 | ||||||
12/22/21 | Fully cleaned up the entire truck outside and inside, including the bed which was filthy with wetness, rocks, mud, bolts, and nails under the flat bed mat that was on top the bed liner. Also washed down engine compartment as there was lots of rat feces & grass & twigs brought in by rats. Saw a rat under the hood as I opened it. Also, should probably park the truck at a rear-downward slope as I think the cap may leak just a little, and water accumulates at the front of the bed if not sloped back to allow it to drain. Horn did not work so replaced with Wolo Maxi Sound 2 Horn Set #320-2T.
They are OK; they are not quite as loud as I'd like. Apparently they are
"150db". Replaced windshield wipers. Brand Carquest XQ20. |
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9/11/21 |
RR tire looses air faster than the rest. |
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3/8/20 | Changed oil and filter; oil = 7qt Rural King 5W20 Full Synthetic; filter=Motorcraft FL-820S.
Engine made quite a clanking sound at startup for about 2 seconds until oil
was circulated. |
116,742 | ||||||
2/23/20 | Mileage logged. JCA will be using it for work this week. Oil needs to be changed. 3/2/20> Calculated that the 4 days I used the truck for work commute I
got average of 12.5mpg. |
116,558 | ||||||
approx 2/17/20 | AKA had battery replaced. Duralast 52948596046 which appears to have a 2 year warranty. |
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1/16/20 to 2/4/20 |
Trip to Rhode Island & back |
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12/15/19 SUN |
Coolant recovery tank coolant level has not dropped at all. |
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12/9/19 MON |
Coolant recovery tank seems to be holding coolant now. To keep observing. |
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12/8/19 | Current tires on vehicle are Mastercraft Courser HXT Size: LT275 65 R18 Tires are worn evenly. There is a spare under the bed. Topped off coolant recovery tank again. Inspected underside extensively: Topped off air in tires to 35lbs. Checked oil again: It is a bit overfilled. |
110,975 | ||||||
12/7/19 | Cooling system has a lot of orange sludge in it and the coolant is orange/rust colored. Cleaned out coolant recovery tank and topped off coolant. Searched internet forums. About half say the sludge is normal, and the other half say it is not. Oil seemed to be a bit low so added approx 1/2 qt RK 10W30 conventional oil. Tested 4WD (4H & 4L): It works good. I believe the high-speed road noise is coming from the differential
(or transfer case?).
Should pull diff cover at some point and at the very least change the fluid.
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12/8/19 | Vehicle seems like it may be losing some coolant. |
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12/5/19 THU |
AKA found vehicle on Facebook advertised for sale. We went to Port Charlotte to inspect it. Fuel filter underneath is shiny (and therefore likely new-ish). Coolant overflow tank has orange sludge in it. No sign of water in the
oil. Noticed lots of noise seeming coming from tires at 50mph + (No not the tires). Purchased vehicle from Terry. |
Approx. 110,895 |
Maintenance Items Cross Reference/ Specs
Fuel tank 27gal (or 30 possibly but likely 27)
Coolant: "Motorcraft Premium Gold Engine Coolant with bittering agent
(yellow-colored)"
"VC-7-B / WSS-M97B51-A1"
The Zerex G-05 is suitable coolant compatible with this vehicle.
Door Sticker Tire Size: P275 65 R18
Tire Inflation Pressure (cold): 35lbs front & rear
Oil weight: 5W20
Oil capacity: 7qts
Oil filter: FL-820S
Air Filter: FA-1754
Fuel Filter:
Transmission:4R75E
4R75E note: "-A sealed case and lifetime transmission fluid make the
transmission maintenance free, while adaptive pressure control maintains
consistent shift feel over time."Automatic Transmission Fluid: XT-5-QM /
MERCON V
ATF capacity: 13.9qt
Transfer Case Fluid: XT-2-QDX / MERCON
Transfer Case capacity: 2qt
Transmission Pan Bolt Torque: 10ft lbs (per 2 separate youtube video)
Flex Fuel capable?: Unclear. "If your vehicle is FFV capable, it may have a
yellow colored fuel cap."
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