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2004 Mercury Grand Marquis LS Ultimate - aka "Seacar"
Flooded during Hurrican Ian September 28, 2022 then caught fire, but it still is my daily driver!

Maintenance & Repair Log  |  Features & Specs  |  Home

Maintenance, Repair, & Improvements Log

 

Date Description of Work Done Odometer Parts Cost Labor Cost Total
Cost
Warranty Notes
FUTURE: Future oil change: Add Lucas to oil at 20% Lucas to 80% oil.
5/1/24
Compressor Seized?
(JPOST)

Various advice:
-Get flush from AC supplier: AC Pro Power Clean and Flush
-D New compressor: scroll or piston? OEM or what manuf?  GET PISTON - BETTER.
-Blow out with Jimmy nitrogen
-D Oring kit - Replace orings (20 or more - get a kit) of hose unions. Coat orings in refrig oil.
-3 special orings for condenser (Ford only part)
-D New receiver/dryer.
-D New condenser OEM 3W1Z19712AC (Tascaparts.com)
"aftermarket ones don't fit properly. Been there done that so you don't have to go through with it."
-D Orifice tube
-D PAG 46 oil
-Special tool for AC lines fittings
-Vacuum for 2hrs at least or overnight better.

[Follow Rock Auto instructions for replacement]
 

12/27/23
I injected to various areas of the air intake a full 14oz can of carb cleaner and ran engine at fast speed to clear it out all through the system, all in effort to clean out intake components.
 
191,212
12/8/23
Power Steering Pressure Switch
Sudden failure leaking lots of fluid out.  Kept topping fluid off with Mercon V on the way home.  PS pump was grinding multiple time.
Replaced pressure switch with Duralast PS496 (ended up returning this as a switcharoo).
Refilled with fluid and everything is back to normal.
 
190,856
11/12/23
Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1 quart of Lucas;  filter=Motorcraft FL-820S.  This is the first time I have ever used Lucas.  Engine sounded no different while running after the oil change.  Lots of mysterious grit, as usual, was in the drained oil. Some of the grit was much bigger than sand, the biggest pieces being perhaps up to 1mm in diameter.

11/13/23> This morning at cold startup, the startup rattle that I would normally expect to hear was a bit less then normal.
 

189,540
9/12/23
Flat Tire
Came out to find RR tire low. Found a drywall screw, likely from home, in tire very close to inner sidewall, and I plugged it including rubber cement.

Update 9/13/23> Found tire still leaking at the plug site. Pushed existing plug into tire (couldn't pull it out).  Replugged it drenching the plug in rubber cement: Still leaking.  Plugged it a second time and it stopped leaking for now.  So, there are two plugs in the one area.  If it leaks again I will probably need to get an internal plug/patch or a new tire.

Update 1/11/24
Found tire leaking here again.
 

186,613
9/7/23 Trouble Codes Logged
-P0456 (common, I am unconcerned)
-P0001 ("an issue with the circuit which runs from your engine computer (ECM) to your fuel pressure regulator on your fuel injection rail on your engine"
-C0000 (Possibly related to speed sensor but unsure)
 
9/1/23
Truth be told, I don't see why I can't run straight 10w30 oil in this engine due to hot temps nearly year-round here in FL.
 
8/16/23
C2000 Trouble Code logged
Google: "What Is the C2000 Code? The C2000 code means that the PCM has indicated a fault with the brake switch circuit which is the dedicated stop lamp circuit. The code also deactivates the cruise control system and the transmission torque converter lockup system, as well as the stop lamps on the vehicle."

Another google resource: "The C2000 with Ford means that the car's ECU has tried to open the EGR valve but it cannot get enough exhaust gas into the engine. Some of the issues you'll typically find is rough idle, poor fuel economy, and lack of power in acceleration."

Another Google resource:" C2000 Code Meaning :
C: OBD-II Diagnostic Chassis (C) Trouble Code For Engine
2: Fuel And Air Metering (Injector Circuit Malfunctions Only)
0: Injector Circuit Malfunction - Cylinders
0: Cylinder 10 Contribution/balance Fault
0: Exhaust Gas Recirculation Sensor B Circuit High

The oxygen (02) sensors on your car measure the oxygen in the exhaust to determine how rich or lean the ratio of fuel and air are in the cylinders. Optimizing this mixture means better fuel economy and fewer exhaust emissions.

C2000 OBD-II Diagnostic Chassis (C) Trouble Code Description
C2000 engine trouble code is about Exhaust Gas Recirculation Sensor B Circuit High. Injector Circuit Malfunction - Cylinders and Cylinder 10 Contribution/balance Fault causes most of code C2000.

Reason For C2000 Code
The reason of C2000 OBD-II Engine Trouble Code is Injector Circuit Malfunction - Cylinders.
C2000 DTC reports a sensor fault, replacement of the sensor is unlikely to resolve the underlying problem. The engine error is most likely to be caused by the systems that the sensor is monitoring, but might even be caused by the wiring to the sensor itself."

I cleared the code while driving, and noticed no issue with CC, TC, etc.  Not sure what to think about C2000.
 

8/11/23
Check Engine Light: 3 Codes Stored
P0457 - Evaporative Emission (EVAP) Control System Leak Detected (not worried)
P0456 - Evaporative Emission Control System Very Small Leak Detected (not worried)
B0000 (Something to do with GM vehicle speed sensor, or may be errant code altogether)

The B code is a bit strange. I wonder if it is indicative of issues with my burnt wiring harness near the transmission.

There were no drivability issues to report.
 

8/9/23
Drilling The Key
(JPOST)
 
7/12/23
Intake Leak Discovered
Found that the pipe that goes from the PCV valve to the intake is open & collapsing up by the intake, sucking in air from the atmosphere.  It is quite oily around this compromised area.  This intake leak may be contributing to the rough running engine while idle.
Ordered from Ebay an "Intake Vent Hose Pipe" for 20 bucks.

7/17/23> Received and installed the new Intake Vent Hose Pipe.
 

7/11/23
Blower Motor Failure
Blower motor suddenly just stopped working. 
There is indeed 12v at the blower motor power terminal.  Ohmed out motor, and it is an open circuit.  Replaced with FourSeasons blower UPC 096361769663 from Autozone. Lifetime warranty.

Steering
With engine off, I had Karla rock steering wheel left and right: There is a knock, and there appears to be some play in the central/driver's side rack & pinion mechanism itself.  The noise does not appear to be coming from a tie rod joint.
 

183,888
7/9/23
AC Compressor Noise
The AC compressor is getting noisy which may be indicative of an impending bearing failure.
I am not sure which "type" of compressor I need.  It's either:
Scroll type, or

FS10 type
The FS10 type seems to have a different front clutch than the one on my car. My car seems like it needs the scroll type.

I found that the FS10 type has refrigerant connections in the very back on top where my car has the refrigerant connection on top, longways down the body of the compressor.

There is also an option to go with an upgraded "piston type" but I am not going to go that route, and just stick with scroll at this point.

JPOST

Per this capacity guide.  This car's AC system takes: 7.5oz PAG46 lube, 38.0oz R134A

General Compressor Installation guide.

The Motorcraft brand compressor:
UPC: 031508471924
Model: YCC-151
Part: 5W1Z-19V703-AA

Firestone: Replace compressor, evac, recharge $873.11 (best case scenario)
$1200 if compressor has already started to throw debris (implied condensor & dryer replcment).

Update 7/12/23> Added a can of 2oz PAG oil, and 1oz R134A to system to see if the oil would help quiet the compressor noise, but it did not.  (183,937mi)
 

7/2/23
Cleaned the MAF sensor using brake cleaner and a cotton swab, as prentative maintenance and also to see if it improves idling; it didn't seem to.
 
183,414
5/28/23
Changed oil and filter; oil = 5+1qt Rural King 5W20 Full Synthetic; filter=Motorcraft FL-820S.  Lots of mysterious grit as usual in the drained oil.
There was remnants of perhaps a gasket around the oil drain plug; I do not recall if I made and put on a gasket or not last oil change, but I do recall doing something like that to one of the vehicles in the last year or so.   I reinstalled the oil drain plug withOUT a gasket. To see if it leaks - I tightened it pretty good so I don't think it will leak.

Wait until 190k for next oil change.
 

182,249
4/2/23
Engine Running A Bit Rough At Idle
The engine has been running a little more rough at idle, so to increase the idle, I adjusted the idle set screw out 1 turn counterclockwise. It does not seem to have made a difference but I will leave it this way for now.
 
180,475
1/30/23
Tires
The shaking in the steering wheel is getting bad.  Also I noticed the rear tires are very light on tread.
Since we are in emergency mode and also driving the baby around, I decided to get 4 new tires. Goodyear I believe (unsure what model).  65,000mi
NOTE: These tires MIGHT have Road Hazard on them as the cashier rang it up that way then later refunded most of it, I think without doing a new work order.
Old front tires logged 18,700 mi
Old rear tires logged 38,600 mi
 
178,543
1/16/23
Coolant Issue?
This morning in 45degree cold weather I noticed a little smoke or steam coming up from passenger front of hood.  When I parked I opened the hood, but could not see or smell any coolant leaking.  However, the coolant recovery tank is a bit low.

Update 1/17/23> Coolant level seems fine after car cooled off and I opened cap. It is right at bottom of full cold range.  I topped off coolant to the top of the full cold range.

Topped off power steering fluid from LOW to MAX level with Mercon ATF (not Mercon V).
 

12/23/22
Pulley Noise (while we are staying at Naples hotel during aftermath of H. Ian)
I've been holding a spare brand new Motorcraft idler pulley and belt tensioner/pulley assembly in the trunk.

Due to noise I keep hearing I decided to change out the idler pulley: No change - the noise is still there.
Then I changed out the tensioner/pulley assembly, and the noise went away.  The old tensioner's pulley was rough to spin and vibrated a bit, so clearly this was the noise culprit.
 

176,943
12/21/22
The Trunk spring-brace broke. The trunk is no longer supported and you have to lift the full weight of it and prop it up with a pipe to keep it open.
 
10/21/22
Blend Door Actuator
Last night the BDA was clicking and got stuck on heat.  I was able to finally coax it to cold, then I shut the car off and disconnected the battery.
Today I pulled the EATC and identified a violet wire, but could not identify a black wire (both which supply the BDA motor itself). I decided to cut the VIO wire and sure enough, the BDA no longer reacts to inputs.  If, like a year ago, I turn a corner hard, the BDA hopefully will not shift on it's own and go to heat else I'd have to reconnect this purple wire behind the EATC and try to coax the faulty BDA back to cool.
 
10/16/22
Flooding Damage & Fire
As a result of H. Ian on 9/28/22 the 2004 Grand Marquis was flooded with seawater when the canal rose. The floor boards were full of water when I checked the car. Soon after, I began to scoop out the water and try to flush out the saltwater with fresh water.

On approx 10/2, the car caught fire due to organic debris on the catalytic converter caused by H. Ian. I was able to put out the fire. The fire damaged some components under the car including the transmission shift selector sensor, the forward left oxygen sensor connector, the shift cable boot, the wiring harness that connects to the transmission, the vehicle speed sensor, the two left oxygen sensors, etc, the shift cable protective boot/bellows, and two vacuum lines near the fire wall - one which sends vacuum to the AC controlling what vents the AC comes out of, and the other that controls the automatic release of the parking brake.

I spent 5 hours getting all the debris out of the underside of the car and also doing makeshift repairs so the AC would operate. To date, the floorboards are still wet and the inside of the car smells bad, despite the windows/doors open and a powerful fan aimed at the floor for 2 weeks straight.

Established claim with State Farm.
 
9/28/22
Car was flooded by Hurricane Ian.
 
9/24/22
Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt 5W30 Full Synthetic; filter=Motorcraft FL-820S.  Lots of mysterious grit as usual in the drained oil.
 
174,677
9/8/22
The belt tensioner pulley sounds noisy.  I tried oiling it but no change. I did not spin it independently.
 
9/5/22
Picked up car at airport after being there for almost 2 weeks, and right rear suspension airbag was deflated, so either the right airbag or solenoid is leaking.
 
8/15/22 - 8/18/22
Serpentine Belt / Squeak
Upon trying to identify a squeak under the hood, I took the Dayco serpentine belt off and noticed a 1 foot split in it; it was upon imminent failure.  I put the old belt stored in the trunk back on for now.
I will not replace it with a Dayco belt. Instead I've ordered a Motorcraft replacement.
I also ordered a spare belt tensioner & a spare grooved idler pulley.

Upd 8/16/22> Suspecting the alternator (from Amazon) pulley to possibly causing the squeak and belt damage, I removed the pulley and put the pulley on from the old faulty presumably OEM alternator. 

Update 8/17/22> The squeak did NOT go away as after changing the alt pulley, as evident tonight driving home.  The very wet oily substance continues to appear on the belt's front several grooves.
I washed the entire front part of the engine down.  We'll see where oil reappears the fastest.

8/18/22> Drove 22 miles to work: No oil on belt and no squeak at conclusion of drive. Coming home the squeek was present.
 

8/18/22> Rcvd and installed brand new Motorcraft serpentine belt. 174,071
Also rcvd and storing Motorcraft belt tensioner & grooved idler pulley in trunk along with old undamaged belt. The torn Dayco belt went into the garbage.
 

173,941
7/31/22
No Crank
Went to turn the key to start the engine and got the click click again, multiple times, even though I had  just thoroughly cleaned both battery posts 6 days ago.  I did not notice if the dome lights went out or not.  I disconnected and reconnected the negative post, and then the car started.  Not sure what is going on here but I suspect the starter or starter solenoid maybe be on it's way out - perhaps the starter since the click click is likely the solenoid. Not certain.

8/4/22> Yesterday and esp. today the click click click when trying to turn the key was constant.
I checked the battery's negative shutoff switch and indeed there was significant voltage drop across it.  I took apart the switch, thoroughly removed all grease I put on it and wire wheel brushed the surfaces. I sprayed silicon spray onto the surfaces and put it back together.  Car cranks every time now.  We'll see how it holds up.
 
7/30/22 AC Service
In the heart of the summer, I topped off refrigerant in AC system.  It was nothing scientific, but added 4 or 5 x 10 second blasts of refrigerant which seemed to help inside low temperature blow a little.
 
173,426
7/25/22
Cleaned all battery terminals due to poor connection and car wouldn't crank.  1 terminal was loose.
Terminals were not very corroded at all, as I had last installed them "lifted" off the top of the battery case.
 
6/10/22
While driving at night my headlights suddenly went off.  I turned the headlight switch a couple times and they finally came back on.  Strange.  I believe there is a recall about this regarding a solder joint in the lighting control module.
 Ford will notify owners, and dealers will replace the LCM, free of charge. The recall began April 14, 2017. Owners may contact Ford customer service at 1-866-436-7332. Ford's number for this recall is 15S39.

Video of a guy that repaired his lighting control module: https://www.youtube.com/watch?v=Vr7aR8b45V8  Relay part number he cites: NEC EQ1-11111S
The LCM he has from his video for 2000 GM is 3W7T-13C788-AH which a google search reveals is for 2004 GM.  Alternative part: Panasonic JSM1-12V-5
Update 6/11/22> Today I was trying to make the headlights fail and indeed as I turned them on and off eventually they did not come on when switched on.  I did not hear the click of the relay. 
I removed the LCM and opened it. I identified the hottest relay which corresponds to the same relay in the above video. I removed that relay and wired in a standard 30A SPST relay in place of it.  Put it all back together and reinstalled LCM. All is working properly at this point.
 
5/30/22
I topped off MGM fuel tank with 3.4 gallons 2 stroke fuel extracted from boat which was dated March 2021 and prior.  It seems to run completely fine.
That means 3.4/19 = 17% -  The car is running on 17% 2-stroke & old fuel.

6/1/22 morning> Added 2.1 gal old boat fuel to car.  2.1 / 19 = 11%.
11% + 17% = 28% boat fuel now in MGM fuel tank, and car ran well coming to work today.

6/1/22 evening> Added approx 2.1 gal old boat fuel to car. 2.1/19 = 11%
11% +28% = 39% boat fuel now in MGM fuel tank.  We'll see how car runs tomorrow.

6/2/22 evening> Added approx 2.1 gal old boat fuel to car. That's 11%.
11% +39% = 50% boat fuel now in MGM fuel tank.
Driving home today I noticed "maybe" a slight decrease in acceleration performance. It was really hard to say.

6/3/22> I can't say the car has lost any power.   It runs and accelerates fine.
evening> Added approx 2.3 gal old boat fuel to car. That's 12%.
12% + 50% = 62% boat fuel now in MGM fuel tank.

6/5/22 evening> Added approx 0.75 gal old boat fuel to car. That's 4%.
4% + 62% = 66% boat fuel now in MGM fuel tank.

6/6/22 evening> Car continues to perform fine.
Added approx. 0.7 gal old boat fuel to car: 4%
4% + 66% = 70% boat fuel no wow in MGM fuel tank.

 

5/30/22
171,412
4/14/22
Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt 5W30 mix of conventional & synthetic.; filter=Motorcraft FL-820S.  Lots of mysterious grit as usual in the drained oil.
 
170,025
3/8/22
On a long stretch of highway, at a steady speed of 71 mph, I observed gas mileage under the following conditions:
Windows up, AC off: 26.4mpg
Windows down, AC off: 24.5mpg
Windows up, AC on: 24.0mpg
 
2/26/22?
Shake In The Steering Wheel
This week I noticed a bit of a subtle shake in the steering wheel around 30-40mph.
Jacked up and spun the front tires.  The tires all had some slight out-of-roundness.  I am guessing the shake is coming from a need for balancing.

Spun the rear tires, checking particularly the RR tire looking for any signs of tread separation: It still looks good. Both rear tires don't look bad in any significant way, and, like the front tires, appear to be slightly out-of-round also.

Probably should get a 4 wheel balancing, or let the rear tires wear out (another few thousand miles probably), replace them, and get a balancing at that time. 
 

168,732
2/19/22
The belt tensioner pulley is squeeking at higher RPMs.
Sprayed some lube on it and the squeek went away.
 
2/17/22
Alternator Replacement
Replaced alternator with a defect-replacement rcvd today from Amazon. Same model
Test run shows that alt seems good (so far).
 
168,463

2/13/22
 

Corrosion is forming around battery posts.  Cleaned most of it, then rinsed away with water.
Used wheel bearing grease around the posts to hopefully facilitate a seal (this seems to help on the 97 CV).
 
2/10/22
Alternator Replacement
Rcvd alternator from Amazon.  Noticed there seem to be less windings than the original alternator.  The guage of the windings seems the same.  The windings don't go out as far from the center toward the front and back. Maybe it is a more efficient design somehow.

Measured battery voltage with old alternator vs. new.
With the old alt, while loaded up at idle, battery voltage dropped to 11.96.
With the new alt, voltage was higher (12.3 or 12.4 IIRC).

The dash lights no longer flicker with this new alternator.

Can keep the old alt as emergency spare, and possibly rebuild it with a rebuild kit.

Days Later> The lights go dim a few times at startup, as if the alternator is intentionally cutting out for a second each time.  This alt seems faulty.  Getting warranty-replacement. See Notes- file.
 

168,228
2/8/22
Added 5 or 6 gallons of year-old fuel to tank including about 1 gal which had 50:1 fuel: two stroke oil.
(Car runs the same - no decrease in performance.)
 
2/4/22
Dash Lights Flicker - Possible Alternator Problem
When the headlights are on, and therefore the instrument panel dims, it begins to flicker quite a bit.
To disconnect battery cable for a period of time then reconnect to see if it makes a difference: No, but when I disconnected the alternator the flicker seemed to stop.

Alternator makes a whining sound when main cable is connected.  I think the alt is going bad.  It is probably the regulator, but looking at the winding there seems to be chips on some of them so it is probably best to replace the entire alt with a new one.
It appears to be a Ford 4G alternator.  The label on the alt is 3W1U-AB GCB dated 1/23/04.

Ordered replacement New PG-8313 alternator from Amazon for about $102 + tax.

2/10/22 Update> See 2/10/22 entry above.
 

1/29/22
I tried to run the heat: I slowly raised the temp from 60 to 90, never heard the blend door make any noise, and the temp blow from vents never got warm.  I did give the car time to warm up.  
I don't think the blend door actuator ever moved.
 

1/16/22
 

Height Of truck is exactly 84in = 7ft 0in) (The 4 roof-rack endpoints cause this height).
This is after I removed the ladder rack guides a few weeks ago which made the height 89in.
To clear the opening of the garage, the height needs to be less than 83in.
 
1/15/22


1/6/22> Water Pump Groan
Noticed a whine at certain RPMs.  Removed the serpentine belt, and rotating the water pump pulley reveals a noise and also resistance.  Clearly the bearing is going bad.  No leak noticed yet.  Rotated the other pulleys and none have noise or resistance (the alt had a light occasional squeak).
1/7/21> Ordered Motorcraft PW464 from Rock Auto. Grand total $60.
Notes: Pulley bolts = 10mm
Pump housing bolts = 13mm
Tightening torque for both: 18ft-lbs

1/15/22 167,456> The water pump made little squeeling noise while cold.  To confirm it is still a problem, warmed up car then spun pump and indeed it was making more noise and had more resistance.

I replaced the water pump.  It was fairly simple.  I used a block of wood and a big mallet, and I placed it against the shaft of the pump and knocked it loose with a couple of blows.
I sanded and wire-brushed the inside of the engine water pump recess and rinsed it with a hose.
Refilled and topped off coolant.  Added about a quart or two of new 50/50 coolant.
 

167,456
11/2/21
Front Brake Service
I decided to check the front brakes and found one of the left front pads worn almost to metal.  There was maybe 1mm left.
I changed both front rotors to Raybestos #680110FZN coated.
I change the pads to Duralast Gold #DG931C
I cleaned up the black caliper piston seals/boots to some degree using spray silicon which should be OK for the rubber seals/boots. I also sanded some surface rust on the caliper piston perimeter.
 
165,075

11/1/21
 

Rear Brake Service
It was detrimental to get the rear brakes replaced due to metal on metal on RR (since before 10/21/21).
Purchased 2 X Duralast Brake Rotors #54105 (The Autozone purchase will be  "returned" when I receive the rotors from Rock Auto which I had previously ordered and have not arrived yet.)
I previously purchased ceramic Durolast pads DG932C (lifetime warranty IIRC).
Did the job.  Removed the (apparent) factory rotor retaining tabs and saw no need to replace them as the wheels & lug nuts hold the rotor in place.

Also I cleaned the orange caliper piston seals/boots using spray silicon which should be OK for the rubber seals/boots. I also sanded some surface rust on the caliper piston perimeter.

On both sides, the outer pads were worn much more than the inner pads.  The left side was almost out of pad material so the wear was nearly symmetrical but obviously the right side had worn just a little bit more.

Additionally, it was found that metal filings were sticking to the paint on much of the rear half of the right side of the car, around the back, and on the trunk lid.  I washed the car and extensively used rubbing compound along these areas. I think I got most of it off, hopefully.
 

165,075
10/30/21
Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt Quaker State 5W30 conventional; filter=Motorcraft FL-820S

Drained approx 6qts transmission fluid.
Dropped the pan.  Pan condition:  Magnet was quite dirty with metal filings & sludge.  Fully cleaned the pan with water and soap. Dried it with air gun and hair dryer.
Replaced the transmission filter - Durolast.
Reinstalled pan with same gasket, torquing pan bolts to 11ft lbs (because some of the bolts showed leakage after fill), and added 5qts of new SuperTech Mercon V.  It still seems overfull once again  but I am not concerned.
 

165,044
10/21/21
Front brakes
Right side is grinding sometimes when slowing. Likely need pads and will replace rotors at the same time.
Ordered from Ebay Rock Auto 2 X rotors (different vendors): Raybestos 680110FZN / 887213144895
(These were recommended on both crownvic.net and by Scott McPherson) 
Ordered from Autozone front pads: Duralast Gold Brake Pads Ceramic DG931C

Update 10/28/21
It was determined that it is NOT the front brakes grinding; instead, it is the RR that is grinding.
I will hold these rotors and pads as I believe the front is also nearly due to be changed.
 
10/16/21
AC has been cycling more lately and hasn't been getting as cold as I think it should.
Ran AC. 
Ambient temp: 89F
Low side: 20-22lbs (seems very low)
Added refrigerant and got it to
Low side: 35lbs. I couldn't get it much higher than that.
Inside blow temp: About 52F
 
164,500
9/26/21
The Blend Door Actuator had and episode:
I turned a fast right corner and the temperature blow went from cold to hot very quickly.  I ran an EATC self test and it reported BDA problem.  Eventually it corrected itself.

Note: I am thinking the small plastic drive gear inside the BDA is missing teeth like what happened on the CV. 
I am thinking to identify the wire that powers the BDA and disconnecting it like I did with the CV.
Wire color research:
The 97 CV wires going to the BDA connector are colored: purple, wht on red, yellow, and possibly red.
A 2003 MGM picture of connector shows BDA wire harness connector colors: white on red
unk, Possibly white on purple, dark blue on light blue, green on yellow, green on yellow, blueish or green on red. 
A 2006 wiring diagram indicates: YEL/LT GRN, DK BLU, RED/WHT, BLK, VIO.
It also indicates that the black and violet wires are power for the motor that drives the BDA.
All 5 wires seem run back to the EATC.  At the EATC if I disconnect BLK (#13) or VIO (#11) or VIO(#26), then that should cut power to the motor drive.  There's a 2nd VIO but that should be for AC compressor.  But if I do cut the wire and somehow the blend door moves "on it's own" if it is even capable of that, it won't return without hooking up the wire.
 

approx.
163,760
7/19/21
Wipers still streak windshield so I removed old worn out RainX windshield wipers and replaced with Michelins I had in the cabinet.
 
161,382
7/19/21
Windshield wiper on left side leaves residual water and it is hard to see. Right side also but to a lesser extent.
Windexed and RainXed the exterior windows (windshield, rear glass, 2 front side windows).
 We'll see if that helps. If not, change the wiper blades (they may be 5 years old and therefore long overdue for changing).
 
6/19/21
Replaced RF & LF tires with Goodyear Viva
-Rqstd no valve stem replacement to save the cost, but they may have replaced them anyway.
-Made appointment. Next time make appointment also.
 
159,848
6/18/20
Been noticing the steering wheel shakes. Jacked the car up and found that the RF tire has a lump on the inside tread. Both tires are quite worn so replacing both front tires tomorrow. The tires didn't quite last 30,000mi (rated 60,000mi tires).

Changed oil and filter; oil = 5+1=6qt Rural King 5W20 Full Synthetic; filter=Motorcraft FL-820S

Cleaned out wiper compartment which was packed with leaves from trees at work.
 

159,843
2/27/21
Changed oil and filter; oil = 5+1=6qt Rural King 5W20 Full Synthetic; filter=Motorcraft FL-820S>
This was after car had been run until hot. Oil continues to have quite a bit of grit on the bottom of drainpan.  Where is it coming from?
 
155,745
12/12/20
Changed differential / axel gear lube.
-Old lube didn't look all that bad.
-Gears look good & unworn as far as my untrained eyes could tell.
-Scrubbed differential cover with stainless steel wool until somewhat shiny.
-Installed cover with reusable gasket Lube Locker LLR-F880 from Amazon.
-Torqued cover bolts to 25ft lbs (per suggestion in online forum).
-Added 2qts & 12oz back in, it was overflowing, and some leaked out before I could get plug back in.  I even tilted car to the right to try to get more fluid in.
-Once bolt holding diff tag on was removed, it could be read that the diff is indeed 2.73 (couldn't see the "2" previously).
 
152,807
12/2/20
Whine related to speed 30+ mph coming from rear (peaks at maybe 55mph).
During the Ga trip last month and up to today I began noticing a whine that is coming from the back that varies with speed.  It does not change whether accelerating, decelerating, or no acceleration.  Therefore,  I don't think it is  the differential.  I'm thinking it could be the tires, or axel bearings. 
Or, it is just something I never noticed before.

Differential bolt tag:
V026M
(2?) 73 88 4A27
Door sticker "Axel" code is "C8" which apparently means 2.73 open differential.
The 88 I believe means 8.8inch ring gear (which is important for the proper size differential cover gasket).

Found a good re-useable differential gasket: Lube Locker LLR-F880 will fit my 8.8inch.
(Apparently only RTV has been used by factory for many years).
Ordered  brand Lube Locker LLR-F880 from Amazon

The owners manual calls for "Motorcraft SAE 80W-90 Premium Rear Axel Lubricant 5.0 pints"

Use a 3/8in rachet to loosen the axel lube fill plug.

Jacked up car. (152,465mi)
-Ran car in 2nd gear with wheels off the ground and could not reproduce sound.
-Checked rear wheel "play": Both rear wheels have slight in-out play as I believe should be expected. Not other "play" noticed.
-Checked for signs of axel lube leakage: No signs of leakage at axel wheel bearings. There has been some leakage around bottom of differential cover.
-Checked lube level: Removed fill plug - Lube level is full. Wiped grease off of fill plug magnet.
At this point I am not concerned about axel bearings or the differential.
 

152,465
11/19/20
Car was running bad and posted codes P0171 & P0174 indicating lean fuel/air ratio.
Under head I noticed rubber joiner between PCV valve tube and intake manifold was open and sucking air.  Went to Autozone across the street and got and installed new rubber piece.

Acceleration was poor after this repair likely to computer-learned condition.  Disconnected battery once, then again but this time shorted the terminals. After maybe 45 minutes I reconnected the battery, started car, and blend door actuator started acting up. It was stuck on heat. Ran an EATC diag and got code 024 (IIRC).  Had to disconnect battery again and reconnect and I think it finally calmed down and cold air was blowing.
 

150,233
10/24/20


Changed oil and filter; oil = 5+1=6qt Rural King 5W20 Full Synthetic; filter=Motorcraft FL-820S>
This was after car had been driven. Oil was very soupy and had quite a bit of grit on the bottom of drainpan.
 

150,206
10/06/20
As preventative maintenance, installed new serpentine belt (Dayco #5060910).  This belt has shallower grooves than the original but seems to work fine.

Stored the original belt, which is still in good shape, in the trunk to use as emergency spare.
 

149,419
9/12/20
Battery no longer will crank car.
Replaced battery with Rural King.
(2 yr free replacement / 72 mth pro rated)
Due to lots of corrosion from old battery, replaced negative disconnect switch assembly and positive terminal assembly which required rerouting of some main wires.
 
148,191
8/11/20
Cooling fan problem:
A crack/separation formed on the perimeter of the 6-blade plastic fan.  Centrifugal force at higher RPMs then caused the fan diameter to expand and rub the fan housing making alot of noise, wearing down the edge of the fan as well as the housing, which would evantually lead to additional failures. 

Unable to find just fan blade locally. Replaced entire fan assembly with Dorman 620-120  purchased from AZ grand totaling $192 (to return).
Alt:  (OEM cross ref: 3W1Z8C607AC, 3W1Z8C607BD, 3WIZ8C607BA )
Rock Auto - grand total $117
Amazon $125
Ebay $99, but commonly $125
Best price: Ordered from Rock Auto grand totaling $112 & also has limited lifetime warranty.

Forum Discussion/Notes
 

147,057
5/30/20
1) Exhaust leak repair

First noticed 5/27/20, there is a small exhaust leak again at the union between the right mainifold and cat pipe. Purchased 2 new exhaust flange gaskets Felpro 60924 (AutoZone) & Permatex Ultra Copper #81878.

Decided to take apart both mainfold-to-catpipe unions.  Noticed the nuts on the right studs were LOOSE.  The gasket flaked off the right side in multiple pieces. The left side was still intact but degraded. Went to Autozone to try to find a better donut type gasket but did not. 

Decided to try to use washers & lock washers to help keep nuts tight but did not have enough stud length to get nuts started so abandoned that. Anyway, the lockwashers likely won't help since I believe the degraded gasket material is responsible for the gap to no longer be tight, the leak to occur, and the nut to then be loose.

Used a wirebrush and wire wheel to clean up both sides of each mating surface.  Vacuumed the holes. Cut the new gaskets in a circle and applied Permatex to all sides of mating surfaces.  By the time I was able to get nuts started the Permatex had set. I tightened the nuts very tight. Confirmed no leaks afterwards by spraying water from a hose on the unions and revving the engine.

Tips for next time because this was a bit of a cluster and will likely leak again in a couple years:
-If a new exhaust leak develops, first try tightening the union - it just may seal back up.

-Use a second set of jack stands to hold each cat pipe as they are heavy and only supported on left side by a wire.

-Do not attempt to use lock washers again or any additional hardware on the studs again.

 

2) Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt RK 10W30 non-synthetic;  filter=Motorcraft FL-820S


 

144,230mi
5/24/20 SUN
Car electrical system has been acting odd lately.  Lights go out when car is started, instead of going dim.  Is battery going bad? Battery is 4 years old now (mfg 3/2016)

Decided to clean battery connections. Both positive as well as negative were gunked up with corrosion.  Thoroughly cleaned them, and electrical system seems better now.

Took apart area below windshield wipers and vacuumed & blew out an enormous amount of packed leaves.  This is the first time since owning the car I have cleaned out the leaves from the trees at work.
 

144,169
5/11/20
Partial coolant change out:
-Drained radiator & coolant overflow tank, and pushed out as much coolant as possible with air pressure.

-Refilled with 1 gallon coolant (Zerex ZXG051 spec G-05) , ~1 qt 50/50 (accidental), and ~3 qts tap water for a total of 8 quarts added.

-Since the coolant capacity spec is 19 qts, and the overflow tank was about a qt low, total coolant before changeout was 19-1=18qts.

8 / 18 = 44% coolant changeout.

Need to get 1 more qt of water into system to thin to 50/50, but I doubt it is critical.
 

143,772
April 2020
Due to COVID-19 & subsequent working from home for 4 weeks, car was driven to work only a few times in April.
 
3/8/20
Turned idle screw 1/2 turn clockwise to increase engine idle
(This appears wrong - it should have been turned CCW, not CW.)
 
141,906
2/29/20
&
3/1/20


Purchased and installed Ford Racing M9424P46 Intake Manifold with Fel Pro gaskets.  Changed out the Intake Manifold.  Ran car without belt - it ran good.

24 hours after applying Permatex Ultra Blue #81724 around all water passages, I added coolant and ran car - no leaks.

The old intake manifold had compromises around t-stat, and that is why there was a coolant leak.

See also 2/21/20 entry below.

Update 5/11/20> This repair is holding well, and there are no apparent coolant leaks.
 

141,575
2/22/20
Replaced rear air suspension air springs.
Used petroleum jelly on the orings (later determined that silicon would have been best to apply to orings, not petroleum jelly).

Rear fender height after pumpup:
L  28in     R  27.25in
Hours later:
L 28in      R  27.0 in
 
141,487
2/21/20
 

Discovered dripping coolant leak seemingly coming from driver-rear of intake manifold-to-intake joint.  It appears the intake manifold will need to be replaced.
Dorman 615-175 (not 615-178) seems like common almost-OEM replacement, however, I've read a few bad things about the Dorman such as acceleration hesitation.
I've also read to get the Ford Racing intake for above 2001.

Forum Discussion/Notes

1AAuto How-To

1AAuto Replacement Part $175 free slow shipping.
Complaints about accessing the spark plugs after this is installed.

(See also Notes- file in Vehicle project folder)
(See also 3/1/20 entry above)

Note: There are several COP & fuel injector plugs which no longer snap locked on, so if any misfires occur, make sure all 16 plugs are fully seated.
 

2/2/20
I suspect the RR air suspension bag or connecting tubes is leaking.
Rear fender heights:
2:52pm  L=27.25in   R=28.25in
5:50pm  L=27.75in   R=26.5in
(These numbers seem inaccurate. To get another set of data).

Update 2/17/20> The compressor runs more than often, and I inspected right and left air springs: Right has many cracks in base, and left has a few cracks in base. I am going to conclude that a new set of air springs should solve the problem.
Ordered a new set of airsprings & o-rings from Ebay branded "maXpeedingrods".
These were almost the cheapest I found at $59 for the pair.   Video to replace airsprings.

 

1/18/20
Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt RK 10W30 non-synthetic;  filter=Motorcraft FL-820S.

Drained approx 4.5 qts transmission fluid and replaced with new 5 qts SuperTech Mercon V.
Fluid level is now way way above top of crosshatch. Hopefully this isn't going to be a problem.

Cleaned the MAF sensor.
 

140,046
1/15/20
Replaced both rear tires with Goodyear Viva 3 UPC 697662124986.
Previous RR tire clocked 35,300mi
Previous LR tire clocked 33,100mi

Need to determine best PSI for rear tire wear. I am thinking 30psi.

New standards for tire inflations:
Front: 32psi
Rear: 30psi
 

139,901
1/14/20
RR tire leaking at center of tire tread where it is bald. 
Plugged tire.

RR center of tire is BALD.  Need to replace both rear tires ASAP.
 
139,865
11/24/19
When trying to start car the last week or so, more often than not it has been clicking alot.
There is lots of corrosion around positive battery post again.  Thoroughly cleaned up positive and negative posts & connections, and also added a "separator" to keep some of the battery acid from coming up and making contact with the positive terminal.  The separator is a cutout from the plastic lid of a sour cream container. 

Checked oil level: Good

Checked tire pressures: Topped off.
 

137,764
10/10/19
Found LR tire low & long skinny screw in tire. Removed & plugged it.
 
135,753
9/28/19
Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt RK 10W30 non-synthetic;  filter=Motorcraft FL-820S. I audio-recorded engine's first start after oil & filter change. It didn't seem to make much startup noise.
The old oil had lots of grit settled at the bottom of the catch pan. Concerning. Could it be sand? Or is it something else?

Checked the air filter. It was not seated properly and somewhat deformed. This grit in the oil is likely sand slipping by. Replaced air filter with proper fitting new Fram Extra Guard CA5056.

Update 9/29/19 (135,334mi)>  I cut open the old oil filter but did not find any grit.  Concerned for the possibility of additional grit still remaining in oil pan,  I ran the engine then immediately re-drained the oil in a clean catch pan.  I found no grit as I put the oil back into the engine. We'll see how the oil looks in 5000mi.
 

135,300
8/25/19
Due to ongoing shake at certain speeds, removed both rear tires and inspected for unevenness:
-Both tires roll fine without any indication of wobble or belt separation.
-RR tire is wearing more at the center than the outsides. I did not note how RR tire was oriented to studs therefore it may not have gone back on exactly the same circular orientation.
-LR tire seems to be wearing more toward the center than the outside, but to a lesser extent than the RR tire. I put this tire back on at the same circular rotation.
-Reduced tire pressure in both rear tires to 28lbs in effort to reduce middle tread wear and force outer tread wear.
-Both rear tires will likely need to be replaced in the next 6 months unless wear improves.
(RR  is at about 30k, LR is about 28k).
 
134,009
8/19/19
Went to start car after it sat for about an hour and it just clicked. Tightened negative battery cable switch and then car started.
 
8/17/19

 

Fluids & tires check:

-Battery Water Level: pass
 (positive terminal already has some corrosion starting again)

-Battery Load Test: not checked

-Brake Fluid Level: pass

-Coolant Level: pass

-Power Steering Fluid Level: topped off

-Serpentine Belt Inspection: not checked

-Tires Air Pressure: Topped rears to 35psi & front to 32psi.

-Tires Visual Check: pass

-Transmission Fluid Color & Level: Not checked

Due to ongoing shaking at certain speeds, jacked up the front and spun the tires: They are a little imperfect but not significantly.

8/10/19
Due to ongoing vehicle shaking at certain speeds, checked both rear tires/wheels by jacking up one side at a time and spinning in drive.  Tires do not seem deformed. They still wobble about the same as they did in the past likely due to slightly bent axels from a couple years ago.
 
133,491
7/22/19
Starting Issue
Several times when starting the car today and once over the weekend it would click-click several times then crank and start.
In 2018 it was a loose battery cable.
The battery is over 3 years old now.  (RK replacement battery: 65-60 $60 or 65-72 $75)
Load-tested the battery. It seems weak but not necessarily end-of-life.
There is lots of corrosion on the bottom of the positive battery post. To clean this up and observe.

Evening> Fully cleaned battery top, posts, and terminals. 
Also noticed a gap exists around the positive battery post where presumably some acid has been splashing up and out, causing the corrosion  Used Plumber's Goop in effort to seal this area.
Car cranks and starts fine now.
132,721 mi
 

132,721
7/3/19
Replaced both front tires with Goodyear Viva 3 (RF, LF) 60,000 mile tires.
(The previous front set of tires lasted just over 30k mi. These may also only last this long).
Next time looking for tires check here for
Walmart tires & reviews: https://www.walmart.com/tire-finder
 
131,774
Approx 6.29.19
Corrected tire pressures to:
Front: 32lbs
Rears: 35lbs
& spare

Front right tire is balding. Need 2 front tires.
LF=GoodyearViva3(5/18/17-99,352)
RF=GoodyearViva3(3/27/17-97,100)

Walmart CC
Goodyear Viva 3 60k $66 each, no credit for early wear.
Douglas all season 45k  $54 each.
 

131,618
6/4/19
Windexed and RainXed the exterior windows. 
(Kind of a rush/quick job.)
 
5/26/19
Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt RK 10W30 non-synthetic;  filter=Motorcraft FL-820S. I audio-recorded engine's first start after oil & filter change.

Also sprayed a lot of carb cleaner down the intake on and past the throttle plate.

Cleaned the MAF sensor.
 

130,056
5/16/19
Topped off tire air pressure.
35lbs rears.
32lbs FL
36lbs FR - I added more air on this side since car has been pulling right a bit in effort to reduce drag on the right side. Not sure if this will make a difference.
 
4/21/19
Topped off oil with RK 10W30 (less than 1/2 qt).
 
128,392
3/27/19
Front Right Audible Buzz
Over the last week or two I've noticed a brief and fairly loud audible vibration or buzz coming from right-front a few times while roling.  Is something lose FR?

Forum Post / Discussion
 

3/23/19
Speed/Wheel-Related-Vibration
I've noticed speed-related vibration over the last few weeks.
I jacked each tire up, spun it, and confirmed no significant defects or separation showing in tire tread.
 
127,200
3/10/19
Added some R134A refrigerant to AC thinking it may just need a touch.
 
126,680
2/2/19
Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt RK 10W30 non-synthetic;  filter=Motorcraft FL-820S. I audio-recorded engine's first start after oil & filter change.

Fluids & tires check:

-Battery Water Level: pass
-Battery Load Test: Passed, though almost on the weak side.
Battery had some corrosion on the positive terminal. Wiped it off and applied lithium grease spray to both terminals.

-Brake Fluid Level: pass

-Coolant Level: pass

-Power Steering Fluid Level: pass

-Serpentine Belt Inspection: pass.

-Tires Air Pressure: Topped rears to 35psi & front to 32psi.
-Tires Visual Check: pass. All tires are wearing evently>
 Front tires will likely need to be replaced in the next 6 months as they are quite worn.

-Transmission Fluid Color & Level: pass

 

125,643
1/27/19
Added some brake fluid as the brake indicator light has been flashing once or twice a day.
 
11/10/18
Blinker switch assembly replaced.

Removed and spray greased ignition switch & linkage.
 

11/6/18
Driving home tonight I noticed the blinker would not automatically turn off (both left & right).
Likely the blinker switch assembly needs to be replaced. Ordered new blinker switch assembly.
How to change out blinker switch assembly:
https://www.youtube.com/watch?v=WqWeB_6BOm4
 
11/5/18
Checked most fluid levels & tire pressures
 
9/16/18
Checked all fluid levels:
-Oil: Added 1/2qt RK 10W30 to bring level to top of crosshatch.
 
9/1/18
Plugged RF tire as it picked up a screw.
 

Transmission fluid service & filter change.

-Rotated crank shaft all the way around with a wrench on the crankshaft pulley bolt, and determined that there is no plug on the torque converter to drain the fluid from it. 
-Drained approx. 4.5 qts by removing trans fluid cooler hose and running engine. This sucked the pan nearly dry.
-Determined that there is no other way I could think of to remove additional fluid.
-Replaced filter with Duralast TF403, cleaned bottom of valve body (dirty), cleaned oil and metal filings from magnet, and  installed new drain pan which has a plug in it for easy future draining.
-There was no yellow object in the pan (from factory) so that tells me the pan has probably been dropped before.
-Transmission fluid capacity is approx. 14 qts. 
-Added 6 qts new "SuperTech Mercon V" (overfull about 1.5qt).
 14-4.5+6=15.5
 6/15.5= 38% of the fluid is new. 62% is old.
-To drain pan again (approx. 4 qts, no FIVE quarts since I overfilled it) perhaps at 150,000mi, by simply unscrewing the plug, and add 4 qts or so.
-Car shifts normally as before.

-Topped off coolant overflow tank with perhaps a pint of 50/50. Coolant seems to be slowly getting lost lately.
 

118,147
7/14/18
Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt RK 10W30 non-synthetic;  filter=Motorcraft FL-820S

Old oil was quite dark.
I should probably get back into the habit of changing the oil every 5,000mi again.
 

116,790
7/6/18
Found coolant overflow tank slightly low (1/2inch). Added Zerex G05 pure coolant to bring level to lower cold line on overflow tank.
 
6/2/18
Replaced burnt-out tag light, as I was pulled over last night for it (warning).

Checked all other external lights: All working.
 

5/5/18
Replaced both catalytic converter assemblies with:
EASTERN CATALYTIC 30384 ECO II RIGHT
EASTERN CATALYTIC 30383 ECO II LEFT
Purchased from RockAuto.com; 5yr / 50,000mi warranty.
Flange gasket for left CC-pipe-to-manifold seal: Felpro (Autozone 60924). purchased and cut one for the left CC-pipe-to-manifold seal.  For the right, reused the one I previously installed.
Coated all mating surfaces with Permatex copper.

After removal of the old pipes, looking through the downstream end I could not see any CC material  in the downstream cats, and no material fell out of the pipes. Material must have been blown out of CCs.  While pipes were off, I used a shop vac to check Y pipe for blockage. I also used a piece of romex cable to poke down the Y throat. No blockage was detected whatsoever. The pieces must have made it to the muffler and settled there, or got blown out of the tail pipe.

Replaced upstream oxygen sensors (as preventative maintenance):
2 X MOTORCRAFT DY1401 oxygen sensors
Purchased from RockAuto.com; 24 month warranty.
Loaned Autozone oxygen sensor tool 27110 which was invaluable. 2 of the 3 pieces of that tool were needed to get the left upstream O2 sensor off the manifold.

Re-installed original downstream oxygen sensors (since they do not impact engine performance).

Anti-seize was applied to all oxygen sensors and related bolt assemblies.

Broke-in CCs by running car for about 5 minutes at idle, then 2 minutes at 2k-3k RPM. Shut off to let cool down using fans to cool CCs. Then road-tested it.

OIL LEAK: I noticed that the front of the oil pan seems to be leaking just a little bit.
 

113,970
4/30/18
Installed event recorder (dash camera) at some point after 4/30/18.
 
4/27/18
Right rear cat is rattling and blocked again, and acceleration is drastically suffering.
(See past notes at 7/9/17 entry below).

Forum Discussion / Notes

Unable to knock blockage loose with mallet so drilled 5 X 1/4in holes in side of RR CC to help with exhaust flow.  Car is loud now.
 

4/20/18
Ran the LF tire up onto a curb and put a small slice into the rubber near the rim.
4/21/18> Put glue (Plumbers Goop) onto gash.
 
3/31/18
Starting Issue
Several times when starting the car today it would click-click 1 to 4 times then crank and start.
Solenoid or Starter?
Turned out to be a loose battery cable.
 

Note: Timing chain guide & tensioner invaluable thread.
 
2/27/18
Tire Pressures
Rcvd new tire pressure gauges from Ebay. They seem reasonably accurate.
Found that all 4 tires were way overinflated. Rear tire pressures approached 60psi while front tire pressures were 52psi.
Corrected rears to 35psi and fronts to 32psi. To observe ride behavior.
 
111,367
2/2/18
Removed a screw and plugged hole in LF tire
The screw was picked up in the parking lot adjacent to the Floor Club this morning.
 
110,871
1/20/18
Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt RK 10W30 non-synthetic;  filter=Motorcraft FL-820S

Removed and cleaned MAF sensor.
 

110,284
1/14/18
Checked over fluids & tires:
-Oil is halfway down the crosshatch & I did not top it off.
-Tires were low, so topped them off.

I should change the oil soon.
 

110,XXX
12/24/17
Disconnected & cleaned positive battery terminal & clamp as it had a lot of corrosion on it.
 
12/17/17
Body damage
While backing up in the driveway I accidentally side-swiped Scott's car, damaging the left side-view mirror and scuffing the driver's door on the MGM.   The spring broke out of the mirror housing.  On mirror defrost connector was ripped off the mirror.

I ended up improvising a repair by drilling 2 holes and screwing the mirror to the swivel stalk.   Therefore, the mirror will no longer gracefully swivel. 

Compound easily corrected the driver's door scuffs.

The mirror shakes slightly due to wind pressure at higher speeds.  It is mildly annoying.

The left mirror does not defrost (as expected), and is an annoyance with regard to the morning dew.

Update 12/21/17
I was able to re-insert the spring inside the upper mirror housing, despite there being broken plastic pieces that came off the spring.  The mirror seats perfectly just like it did previous to the accident, and it swivels back with pressure like it should.

I was able to solder a wire to the surface of the mirror where the connector was ripped off.
Between the contacts it measured 180 ohms.  I am not sure if this is what it should measure.
That would mean less than 1 watt of heat is sent to the mirror which seems very low.
It is possible that part of the mirror wont heat, and part will heat, due to how I soldered it. May need to re-solder.  To check to see if indeed it heats enough to remove the morning dew.

Update 12/22/17> Tested the electric defrost system: The left mirror is not heating up. The right mirror got hot pretty quickly.  I likely need to replace the left mirror. Number printed on the back of the mirror itself: G57014368CHABC. This number does not google to anything.
On Ebay found a part number that seems like it might work: 1W7Z17K707AB.

Update 12/24/17> Rcvd mirror ordered from Ebay. It looks identical to the one taken off. New mirror measures 12 ohms on the heater leads. That's more like it. Installed and tested it: Successful replacement.

Update 12/25/17>  I noticed the replacement mirror must be warped slightly as when looking at the reflections it casts there are visual anomalies.

Update 1/6/18> I got a refund for the replacement mirror, then I ordered and received another.  I noticed similar visual anomalies with this one and realized it needed to be fully seated to the mount and the anomaly went away.  Now I am thinking the first mirror I purchased wasn't a problem after-all.  Keeping that first mirror as a spare.

11/4/17
Rotated RR tire clockwise 1/5 of a turn as to try to even out wear from bent axel.
 
107,545
10/27/17
Checked fluids: All OK.

Topped off tires.
 
10/22/17
Had Firestone align car under lifetime alignment policy.
It looks like I had previously adjusted camber into the green (in-spec) on 9/2/17.
Toe was the only item out-of-spec.
 
107,108
10/17/17
Replaced LR tire with Goodyear Viva 3 60,000mi.  The thump/vibration is gone.
 
106,799
10/16/17
There's a thump/vibration the back end again. 
I jacked up car and spun wheels and found LR tire with a lump in it. It seems the tread is separating.
To replace LR tire.

The newish RR tire looks good with just the slight wobble that has been present (likely slightly bent axel).
 

9/7/17
Replaced both rear shocks with Monroe #5993 since they were cheap after rebate.
Old shocks showed no sign of defect.
 
105,242
9/3/17
Changed front coil-over-shock assemblies.
Monroe "strut" 171346 lifetime warranty.

How To: https://www.youtube.com/watch?v=PZoH5UV3v80
"You went the long route to doing that. All you really need to do is to undo the upper control arm ball joint from the knuckle and the sway bar end link. Once those are cleared out of the way undo the coilover and you can get it out." 
This is what I did. Also removed the brake calipers.

The right upper ball joint allen hole is getting stripped out because I did not have the right size allen wrench.  Instead, I used vice grips to hold the upper ball joint around the boot on both sides (boot already was torn on both).

Car drives better now and does not seem wandery at high speeds. However, right side still sags just a little.  It seems that the RR shock may need to be replaced. To investigate.  Forum Discussion/Notes
 

105,100
9/2/17
Frame evaluation:
Put car on jack stands on all 4 corners of the car on the frame inside the wheel spread.
Measured from the driveway up to numerous places under the front of the car: The was no difference in measurement at most of the points, and only a slight difference at a couple of points.
I have concluded that the frame is not bent.

Right & left side camber adjustment. Removed tab on camber adjustment bolt so that there is more room to adjust camber.  Adjusted right camber all the way in.  Adjusted left camber in half way but not all the way.  Adjusted by sight and by using a level. It seems pretty close.

Subsequently, right & left side toe adjustment. Used tape measure to measure distance between inside of tires front of tires vs. rear of tires and got toe pretty close.  There may be just a small bit of toe-in now.

I am now thoroughly convinced the right-front lean is due to faulty coil over shock assembly. To change both coil over shock assemblies.
 

105,702
8/26/17
The car shakes a bit at times around 51 and higher speeds still.

I am concerned that the RR axel is bent.  As a test ,I swapped RF and RR wheels since RF wheel  & tire seems to have the least out-of-roundness of all, and I concluded that the RR axel seems bent. LR seems slightly bent and matches that of both sides of the Crown Vic which I checked for comparison purposes.  Put back on RR wheel strategically in effort to counter the axel wobble.  If I take the RR wheel off again, try to put it back on the same by marking 1 lug and 1 hole.  Theoretically I should try to keep the RR wheel on that spot always.

Hopefully this axel wobble does not mis-wear the new RR tire.

Installed new acorn lug nuts on remaining 3 wheels (RF, RR, LR) to complete the better style lug nuts on all 4 wheels.  These are better because the original lug nuts were thicker, and my 4 way lug wrench kept binding on the wheels when trying to get the nuts off.  The wrench size of these new nuts is smaller (19mm / 3/4in), so keep appropriate lug wrench in car.
 

8/23/17
Had RR MasterCraft tire replaced due to shake coming from that tire.
Goodyear Viva 3 60,000mi warranty installed.

Kept old tire for inspection: No obvious deformity with tread. To inspect tire  further and also rim. Also, check for more or less right-pull.

Handling:
It still has issues with handling at higher speeds.

The old tire has a noticeable defect when it rolls: It dips to one side in a particular area, but deformity is not noticed visually.

RR Rim inspection: Rim seems ok. Not sure

 
 

104,602
8/20/17
Found that muffler patch goop has come off of two holes in LR catalytic converter. Rplcd holes with screws.

Changed oil and filter; oil = 5qt Rural King 5W20 Full Synthetic + 1qt RK 10W30 non-synthetic;  filter=Motorcraft FL-820S
 

104,465
7/9/17
Checked & corrected all tire pressures, fluids, and exterior lights.
Left brake light in center brake light fixture was burnt out so replaced both bulbs with Sylvania #579
 
102,242
7/9/17
Right side downstream catalytic converter exhaust rattle is getting excessive.
Considering to either replace the pipe, or cut open the CC and remove the contents.
Forum Discussion/Notes

7/15/17 update> I removed heat shield from right rear CC.  Yesterday, I hit the brakes hard, and now the rattle is no longer present.  I am refraining from drilling any holes in the CC unless rattle returns.

7/26/17
The rattle returned days ago.
Put a screw through the RR cc.
Discovered that the LR CC is rattling also.
Put a screw through it. The rattle stopped but came back.

Options:
a) Cat delete pipe
*Hard to find
*expensive
*Exhaust will be louder
*Exhaust may smoke
  (Youtube of a pre 97 showed lots of smoke. Youtube of a 2004 showed no smoke.)
*Will there be an issue with lack of backpressure? Mustangs need a tune of some sort when cat delete is implemented.

b) Replacement aftermarket cat pipes approx $120 each.
*The most difficulty will be getting the rear bolts loosened.

c) Replace both rear CCs.
*May be difficult to maintain seal unless pay for welding.

d) Continue putting in screws.

e) Cut and bend open flap on CC, remove CC material pieces, bend close, and seal with VersaChem muffler & exhaust sealer. However, there may be a drone noise due to missing material in cat.

f) Cut out CC and replace with straight pipe, 2 clamps, and VersaChem Muffler & Exhaust Sealer.
 

7/27/17 update>  I put many screws through the CC and it helped for the first 5 minutes then the rattle came back. This is a fruitless effort.

Can I remove the CC pipe assembly, turn it vertical and shake out the pieces? Only if there is not a screen in the output of the rear CC.
Forum Discussion/Notes

Replacement CC assemblies are cheapest on RockAuto.com:
EASTERN CATALYTIC 30383 ECO II Left
EASTERN CATALYTIC 30384 ECO II Right


7/28/17
Rattle ceased this morning. Odd.

7/30/17
Found that there appears to be no more material in RR CC.

Found that there is still lose material in LR CC, though it is not rattling at all.

Patched 1 screw hole on RR CC and 2 screw holes on LR CC using VersaChem 10161 Muffler & Exhaust Repair. To test endurance.

4/27/18
Right rear cat is blocked again and acceleration is suffering. Need to do something ASAP.
Notes to resume at 4/27/18 entry above.

 

102,742

Changed oil and filter; oil = 1qt Shell 5W30 (old-been sitting in garage cabinet for 20+ years, 5qt Rural King 5W20 Full Synthetic;  filter=Motorcraft FL-820S

Note: I have many 5qt jugs of RK 5W20 Full Synthetic oil, so I will be using this mostly from now on until stock has been depleted.

Note: Lots of grit and small pieces of what looks like black paper gasket present in oil, but some of that may have fallen out of the oil filter when I dumped it in the oil drain pan.

MAF: Cleaned MAF with carb cleaner and cotton stick.

Air temp sensor: Cleaned air temp sensor with carb cleaner.

Air filter: Thoroughly blew out air filter.
 

100,103
5/22/17
During round trip to West Palm & Miami this weekend it was observed that at higher speeds when the RF hits a significant deformity in the road, there is a shake/vibration in the wheel still.  Almost a bump-steer but not exactly.

Adjusted LF and RF toe out almost all the way back to the way Firestone adjusted it. 
Currently it is estimated that there is just a little bit of toe-in.

Removed basic / incorrect wheel nuts from LF Ebay replica rim, and installed bulge acorn wheel nuts which fit much better.
Note: Keep universal lug wrench in car since these new wheel nuts are of a different hex socket size.

When front of car is jacked up in center of pillar under engine, car leans right.
This would imply that the RF is heavier than the LF  (or that the frame is bent?).
Forum Discussion / Notes
 

100,011
5/18/17
Purchased GoodyearViva3 tire and mounted to new replica rim, and assembly placed on LF hub.

The current car tire config is as follows:
LF=GoodyearViva3(5/18/17-99,352 on Ebay replica/new rim)  
RF=GoodyearViva3(3/27/17-97,100)

LR=Sumitomo (6/24/14-82,246 on Ebay RIM 4/7/17)  
RR=Mastercraft (1/6/14-73,382)

Note: The Ebay replica/new rim will need bulge acorn wheel nuts (on order from Ebay), as the current basic wheel nuts don't seat properly and bind in the mount holes.

Note: Wheel nut size for this car is "1/2-20".

Car pulls right slightly with current config, however wind has been blowing right also.
Car tested to 68mph and is much less shaky and feels more stable. To test further.

Car is now in suitable condition for a trip.

Future: To reduce toe-in back to spec. and observe.
 

99,352
5/17/17
Tire rotation:
*Placed RR (Goodyear Viva 3) onto RF to match tomorrow's purchase of another Goodyear Viva 3 for LF.
*Placed RF (Mastercraft in bad shape with cupping) onto LF.
*Placed LF (Mastercraft in fair shape) onto RR.

Car pulls to the right.
 

99,344
5/12/17
Rcvd replacement replica wheel from Ebay.
Found that center cap will not fit center portion of wheel as center portion of wheel diameter is smaller than center cap diameter.
Used grinder to grind outer edge of 1 center cap, and now it fits. This grinded center cap has to stay with this wheel.  Marked both accordingly.
Wheel along with a new tire will be mounted to car at an undetermined time in future.

The weight of this wheel is 21lbs.
The weight of an OEM wheel from the car is 19.5lbs.
 

5/10/17
Continued nervous and wandery steering instability at higher speeds.
Blown RF shock? Bad spring? (RF sits lower than LF).
Forum Discussion / Notes
 
5/9/17
Tire rotation:
Placed spare tire on LF: Car still pulls to the right, although less.

Removed spare tire. Swapped LF & RF: Car pulls left slightly.  Likely need to replace RF rim, and tire. Rim is definitely deformed, and tire seems cupped.

The current car tire config is as follows:
LF=Mastercraft (more tread than RF) 
RF=Mastercraft (less tread than LF & deformed rim & cupped tire)

LR=Sumitomo (lots of tread) on Ebay RIM 4/7/17  
RR=Goodyear Viva (new as of 3/27/17)

Car pulls left slightly with current config.
 

98,866
5/7/17
In effort to correct the water leak in the LF side marker lense, I managed to ruin it after pourning rubbing alcohol into the lense.  A replacement lense has been ordered for $31 from Ebay.

Update 5/12/17> I received, and replaced the LF side marker lense.  The front (blinker) socket was a loose fit to the front hole of the new lense.  I cut 2 layers of cork gasket to match the existing socket gasket and attached the socket to the lense. When I did so there was a crack sound, but upon inspection, nothing looks cracked.  Informing Ebay seller.
 

4/28/17
Took apart EATC and replaced vacuum solenoid o-rings with #007 red silicon o-rings from Ebay.  Sprayed o-rings with silicon.  The old o-rings didn't look bad other than they were a bit stiff and had shrunk just a little.  No cracks in plastic housing noticed.
Tested: So far vacuum seems to be holding under heavy acceleration.
 
98,462
4/27/17
Checked all fluids: Good as is.
 
4/22/17
Adjusted toe inward: Turned right & left tie-rods approx 1/8 turn.
Steering nervousness seems reduced.
Right side pull has not changed.
 
98,180
4/19/17
Right-pull is still present.
Did 3 separate tire rotations:

1) Swapped RF (Sumitomo) with LF (Mastercraft). 
LF is now Sumitomo, RF is now Mastercraft:  Car pulls to the LEFT now. The pull followed the Sumitomo tire - interesting.

2) Swapped LF (Sumitomo) with LR (Mastercraft).
LF is now Mastercraft, LR is now Sumitomo.
I do not recall which direction the car pulled after this rotation but I think it was left  but only slightly.

3) Swapped LF (Mastercraft) with RF (Mastercraft).
LF now has a little bit less tread than RF but both are Mastercraft.
Car pulls to the right.

The net change after the above 3 rotations is that the LR (Mastercraft) was swapped with the RF (Sumitomo).
LR is now Sumitomo, and RF is now Mastercraft.

The current car tire config is as follows:
LF=Mastercraft (worn tread)         
RF=Mastercraft (more tread than LF)

LR=Sumitomo (lots of tread)
RR=Goodyear Viva (new as of 3/27/17) on Ebay RIM 4/7/17

Sumitomo is "Sumitomo Touring LST"
 

4/19/17
Sometimes under acceleration, AC blow switches from dash vents to floor to sometimes defroster.
It is likely that EATC orings may need replaceing (Forum Thread). If need be, purchased silicon orings size 007 from Ebay. Coat them in silicon dielectric grease (or plumber's grease). 
Also, the problem could be cracked valve body within the EATC. It is possible that it can be epoxied.
(O-rings replaced 4/27/17 - above).

The other cause might be a faulty vacuum check valve located on the firewall.
Update> I sprayed lots of silicon into the vacuum tube leading to the vacuum check valve with the engine running.  If the problem is with the VCV, perhaps the silicon will help.
 

4/14/17
Front End Alignment by Firestone. Lifetime policy.
Camber and toe were out of spec. Toe was brought into spec. Clerk said camber is not adjustable, even though I later found out it is, and moreso with a kit (SPC Performance Camber/Caster Bolt Kits 87365 /
Install video ).

Forum Discussion / Notes
 

97,839
4/13/17
Alignment Inquiries

Campbell's: $90

Bob the mechanic (works for Campbell's) 887-0115: Unable to contact.

Tire Kingdom: 9450031 s/w Steven:  $90  6 month Warranty
Suggested to swap the front tires and see if pulling changes.

Firestone CCPKWY 205-2021: jerry 84.99 one time, or $169.99 lifetime (on sale) (as long as i own the car). Jerry said bent rim or balance issue will not affect alignment.
Alignment can be done at either Firestone or Tires Plus nationwide.
Deciding to go with Firestone lifetime alignment.
 

3/28/17
Adjusted throttle set screw 1/4 turn outward (counter-clockwise) to increase idle slightly due to ongoing annoying engine vibration at lower idle.  See also 10/26/16 entry.
 
97,130
3/21/17
Shake in car from 30-32mph noticed over the last few weeks.
Either tire imbalance, or issue after brushing the curb with back tires.
(Update> Or likely hit a speed bump going fast).

Update 3/21/17  96,845mi> Jacked up RR, and LR separately and put in gear. Spun wheels and carefully observed: I could not find any significant issue with rear tires or wheels.

Raised RF and LF separately. Spun wheels by hand: Noticed RF tire is a bit more imperfect than the rest.  The inner edge has what seems to be a raised area and a dipped area.  This could be the cause of the shake.

Update 3/23/17> I noticed I must hold the steering wheel a bit left to continue to go straight.  Also, the RF outer wheel rim is flattened in an area, indicating perhaps it had once struck a hard object. Replace wheel? Get alignment? 

Update 3/25/17 97,000mi> Swapped RF tire with spare and shake was gone.
Rotated RF with RR tires and shake is still present with same intensity.
To replace bad Mastercraft tire which is now on RR.
225 60 R16  98T

Update 3/27/17> I went to Walmart and had (RR) tire replaced. They replaced wrong tire and I caught it while car was still in garage.  They fixed the mistake, but placed the other car tire (Sumitomo?) onto the rim with the deformity.  I drove around town and thought the problem was fixed, when in fact the vibration came back and I clearly observed that the rim with the deformity is definitely bent. I need to get a replacement unbent rim.  I kept the old Mastercraft tire as I doubt it is "bad" afterall. The rim OEM part number is apparently:
3W33-1007-AA
3W3Z1007BB

(I eventually used the old Mastercraft tire as a spare tire for the 97 CV).

3/28/17 97,130mi>
Adjusted toe on RF wheel just over 1/4 turn to bring toe in (when facing forward looking right, turned tie rod clockwise 1/4 turn). Originally turned 1/2 turn but that was too much and caused steering wheel to be more towards the right. I did this because I think whatever caused the RF wheel to become bent  I assume the toe went outward slightly. Steering still pulls slightly right but steering wheel is a little more straight.  I hope this adjustment won't prove to be a mistake.

Update 4/7/17 97,496mi> I previously ordered a used rim from Ebay, and today I had the rim swapped and tire/rim combo balanced at Walmart.  The shake is gone. However, the pull to the right is still present. I next need to  consider getting an alignment.

Forum discussion / Note: '04 MGM - Shake Between 30-32mph

Update 4/10/17> There still is some shaking. The LR tire seems the be out-of-round the most.

Forum discussion / Notes: '04 MGM Needs An Alignment - Questions 
 

96,775
3/20/17
Check Engine Light illuminated
P0442: "Evaporative Emission Control System Leak"
I'm not too concerned with this. Tightened the gas cap and cleared the code.
 
1/8/17
Checked all fluids.

Checked all exterior light bulbs

Checked and topped off all tires (except spare)
 

94,278
12/17/16
Changed oil and filter; oil = 1qt Peak Full Synthetic 5W30, 4qts Mobile Super 5W30, 1qt Quaker State 5W30;  filter=Motorcraft FL-820S
Note: I'm making a habit of putting on 1 qt of full synthetic each oil change now moving forward.

Added fluid to power steering reservoir to raise level which was just below MIN to MAX.
Used Mercon ATF (not Mercon V ATF) per owner's manual.

With regard to the knock sound that happens when power is suddenly added and removed:
*Checked the 4 torque converter to flex plate nuts and they all are tight.  Confirming the count to be 4.
*Jacked up the rear end and checked U Joints: The is no play.  The transmission is also bolted firm.
Ran the motor in drive and was able to duplicate the sound.  It seems to be coming from the transmission but still it is difficult to tell. It is an intense knock when witnessed under the car.

Noticed the torque converter does NOT have a drain plug in it.
 

93,116
12/14/16
OIL VISCOSITY RESEARCH
I have questioned the reasoning behind why this car's specs calls for 5W20 oil, when older 4.6 engines call from 5w30 oil (such as my 97 CV). I've studied this and other threads, and at this time conclude that 5W30 is fine for the MGM here in FL.
 
10/26/16
Adjusted idle set screw
1 & 3/4 turns CCW
to raise hot-idle-park-ac-on RPM from about 640 to 700
to see if it helps with slight rough idle.
Forum discussion / notes

Update 10/27/16> Idle doesn't settle down so turned set screw 3/4 turn CW, for an overall net of 1 turn CCW.

At some point after this I adjusted the set screw back to its original setting.
 

10/26/16
Analysis of RPMs based on past ODBWiz logs

CV Idle in gear        MGM Idle in gear
580 (datalog 739)  560 (datalog 151)
580 (datalog 628)  554 (datalog 854)

CV idle in park       MGM idle in park
824 (datalog 739)  645 (datalog 151)
823 (datalog 628)  640 (datalog 854)
 
10/17/16
Re-adopting manufacturer recommended tire pressure.
Adjusted front to 32lbs
Adjusted rear to 35lbs
 
10/2/16
Exhaust Repair
Over the last few days I have been smelling exhaust again when first starting the car. Took apart driver's side cat pipe to manifold union, cleaned it up, and applied Permatex Ultra Copper and tightened the joint.  Then I discovered the right side joint is indeed leaking as exhaust pressure was making the flaking Permatex flutter.  Took that union apart (and had to take driver's side apart again to allow passenger side cat pipe movement). Cleaned surfaces and cut to size a Felpro flange gasket (likely Autozone # 60924), coated it in Permatex Ultra Copper, then reinstalled both the driver's and passenger joints at the same time to avoid any twisting of the pipes.  Joint is sealed once again.

UPDATE 10/14/16: Seal is holding good. No more tick or exhaust odor.

Forum Discussion / Notes
 

9/27/16
Blower motor suddenly stuck on full speed. Will not shut off without turning the key off.
Reset computer:
Found a Youtube video that outlines how to diagnose the EATC (Electronic Automatic Temperature Control) system. 

Forum post that discusses how to replace blower speed controller.

Forum post detailing the BMSC module.

No EATC trouble codes reported, and now blower stays on LOW when shut off.

Determined that indeed the BMSC (Blower Motor Speed Controler) was faulty. Removed old one and replaced with new one: Duralast JA1710 .
 

9/24/16
Passenger side exhaust manifold-to-cat pipe maintenance:
Removed nuts and pulled pipes apart then smeared and sealed joint using Permatex Copper rated to 700 F.
This repair appears to have sealed well as there is no longer a passenger side tick upon hard acceleration.  We'll see what the longevity is, but someone said they redo their Permatex every 6 months.
Forum Discussion / Notes

Note: There is a faint left-side tick only when cold.  The tick is almost completely gone when the manifold heats up (and likely expands).

There is also a rattling sound coming from under the car in the area of the right catalytic converter pipe assembly. 
 

89,142
9/1/16
Filled gas tank with 87 octane and added 1 X 15oz bottle of Red Line Complete Fuel System Cleaner # 60103 to fuel tank.
 
88,164
8/31/16
Installed new Rain-X windshield wipers.
 
8/28/16
Re: Car runs rough during idle.
*Pulled IAC and cleaned it.
*Checked resistance of COP primary coils: All matched at about 1/2 ohm.
*Pulled each COP power connector while running and observed equal change in engine behavior among all 8 COPs.
*Checked for vacuum leaks: Found none.
*Sprayed carb cleaner around base of upper intake where it meets lower intake, again, and observed no change in engine behavior.
*Disconnected a hose from a port on the intake plenum and sprayed almost 1/2 can Gumout Carb Cleaner in short blasts into port while running engine. Finally stalled out engine. Disconnected battery (to reset computer). To let it sit overnight.
 
8/26/16
Car runs slightly rough during idle.
Forum discussion / notes
 
8/24/16
Changed LR door lock actuator.
Installed Dorman 746-188 purchased from Ebay. However, the part number on the actuator itself is scratched off in 2 places.
 
8/22/16
Changed fuel filter.
Installed Fram G8018.
Note: The clips that came with the new filter are too big to fit.  Went to Autozone and bought other clips but they don't work either.  Ended up using zip ties instead of clips.  They should substitute just fine.
Fuel from old filter poured out clear from incoming side (no dirt noticed).
 
87,713
8/20/16
Pulled all 8 spark plugs while engine COLD. They all look evenly worn and are gapped toward .060. Replaced spark plugs with same: Motorcraft Platinum AGSF 32PM. Gapped to slightly less than 0.054.  Sprayed a squirt of WD40 onto threads to get them started, and torqued to just past 15 ft lbs.

Cleaned all fuel injectors by using low voltage to open them and sprayed carb cleaner through.

Car idles somewhat smoother than before.

Need to replace LR door lock actuator. Ordered part.
 

87,6XX
8/13/16
Pulled and inspected spark plug from cylinder 5 (cold engine). Plugs looks worn. Gap is 0.060.
Motorcraft Platinum AGSF 32PM
Sanded electrodes on plug (did not adjust gap) & reinstalled plug to 15ft lbs.
Forum discussion / notes

Cleaned MAF and temperature elements.

With throttle fully open (engine off), sprayed carb cleaner down throat of intake (10-15 seconds) then ran car.  Throat was crudded.
 

8/10/16
Window tinting performed by Suntamers. Darkest legal in Florida.
Solar Gard HP Supreme 30 installed to front 2 windows.
Solar Gard HP Supreme 16 installed to remaining rear windows.

Spray painted right-rear bumper chrome which was mostly chipped off.

Created and installed 120v wiring for power taps at front passenger seat, rear seat, and trunk.

Created power tap off of rearview mirror wiring for radar detector
Update 8/16/16> I noticed power is cut off when car is put in reverse.
Update 8/22/16> A few days ago I tapped into the 3rd wire which was determined to be hot independent of the shifter position.
 

8/9/16
Determine if car is pre-wired for DRL.
Forum Link
DRL Module is F6SZ-13B218-AA

Programmed Homelink button to open and shut garage door.
Forum Instructions extracted from Homelink Instructions.
 

8/8/16-8/9/16
Installed 40A circuit from battery to passenger front seat for inverter.  Designed and installed switched (lighted) ignition override control circuit for inverter.
 
8/6/16
Changed oil and filter; oil = 5qts Quaker State 10W30 & 1 qt Rural King 10W30;  filter=Motorcraft FL-820S
Old oil was quite black, and oil oil filter had some rust on it.
Note: Oil filler cap calls for 5W20 oil.
Note: Oil capacity is 6 qts.

Installed a battery disconnect switch.

Waxed car with McGuires wax.

The bottom of the differential cover has some apparent leaked oil from the past.  Checked differential oil level:  Some came out of the fill port so that means it is full.

The underside of the trunk had patches of surface rust, so wirebrushed, sanded, and gray-primered the underside of the trunk.

Checked air filter: It is moderately dirty and no need to change it for at least 10-20,000 miles.

Sprayed lube over rusty area under the hood such as brake lines, EGR, and blower motor in effort to slow any further rusting.

 

87,416
8/5/16
Completed the deal and took delivery of the car.

Used warm/hot water and thoroughly washed engine compartment and underside of car including within frame holes and crevices. Lots of sand came out of the crevices.

Used rubbing compound on body chrome and got rid of corrosion/pitting.

Replaced LR brake light bulb.

RainXed the windows.
 

87,414
8/2/16
Title & bill-of-sale signed by KJ.
 
7/31/16 Made verbal agreement to purchase car.

Noticed Delayed reverse engagement when putting gear shift lever in reverse, but not more than 2 seconds as the TSB describes.
Forum Discussion / Notes (JPOST)

Forum Discussion / Notes (other poster)

 

FROM THIS POINT DOWN OCCURRED UNDER OWNERSHIP OF KJ
4/20/16
New 5 year battery installed from Walmart.  MAXX-65S
 
87,237
6/24/14
Mount & balance 1 new tire for the passenger right rear tire (with new wheel customer supplied wheel/Rim) by Wilson's automotive in Cape Coral.
KJ said she previously took it to George's Garage because tire kept losing air, and George's said it is because of a bent rim. 

Sumitomo Touring LST (Replacement tire? Went where?)
 
82,246
2/26/14
Pennsylvania title issued to KJ.
 
82,000

FROM THIS POINT DOWN OCCURRED UNDER OWNERSHIP OF IH.
 
unk date
Right side catalytic assembly replaced with
"EM 70380 ECO 11 03/<unreadable>" which is apparently brand "Eastern Catalytic".
 
1/6/14
4 New tires installed by Jack Williams Tire & Auto Service Centers
Mastercraft MC-440

Wheel alignment.
 

73,382
12/13/05
Pennsylvania title issued to IH.
 
11/14/2005
Vehicle purchased Certified Preowned by IH from Mullinax Ford-Mecury in New Smyrna Beach, FL. for $19,750 (minus trade-in plus tax & fees).
 
12,652

FROM THIS POINT DOWN OCCURRED UNDER OWNERSHIP OF ORIGINAL OWNER
 
8/12/05
"Check out for cup holder fell apart CC33"
"Cup holder broken FP5404810 code 01 V.C.C. replaced cup holder and ashtray assembly. Auth # PAAGN"
 
1/24/05
"Customer states that front wipers are streaking"
"Wiper blades replace front wiper blades"
 


 

 

Maintenance Items Cross Reference/ Specs


Fuel tank: 18 or 19 gal
Coolant: "Motorcraft Premium Gold Engine Coolant with bittering agent (yellow-colored)"
The Zerex G-05 is suitable coolant compatible with this vehicle.
Coolant capacity: 19qt


Door Sticker Tire Size: Tires: P225 60R16
Tire Inflation Pressure (cold):
Oil weight: 5W20
Oil capacity: 6qts
Oil filter: FL-820S
Air Filter:
Fuel Filter:
Automatic Transmission Fluid: Mercon V
ATF capacity: 13.9qt
Transmission: 4R75E (to confirm)


 

 

 

 

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